MINUTES OF XXXVII MAINTENANCE STUDY GROUP (ELECTRIC …

76
GOVERNMENT OF INDIA MINISTRY OF RAILWAYS MINUTES OF XXXVII MAINTENANCE STUDY GROUP (ELECTRIC LOCO) MEETING HELD AT SHIMLA (UMB DIVISION), NORTHERN RAILWAY ON 24 th & 25 th JULY’ 2015 RESEARCH DESIGNS AND STANDARDS ORGANISATION MANAK NAGAR, LUCKNOW 226 011

Transcript of MINUTES OF XXXVII MAINTENANCE STUDY GROUP (ELECTRIC …

Page 1: MINUTES OF XXXVII MAINTENANCE STUDY GROUP (ELECTRIC …

GOVERNMENT OF INDIA

MINISTRY OF RAILWAYS

MINUTES

OF

XXXVII MAINTENANCE STUDY GROUP

(ELECTRIC LOCO)

MEETING

HELD AT

SHIMLA (UMB DIVISION), NORTHERN RAILWAY

ON

24th

& 25th

JULY’ 2015

RESEARCH DESIGNS AND STANDARDS ORGANISATION

MANAK NAGAR, LUCKNOW – 226 011

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LIST OF PARTICIPANTS

Railway Board:

S/Shri

1. Navin Tondon, ML.

2. Man Singh, AML.

3. Ved Pal, Advisor/RS

4. Sumit Bhatnagar, Director/RS

RDSO

S/Shri

1. O. P. Kesari, EDSE (Co-ord).

2. A. K. Shukla, EDSE.

3. A. K. Rastogi, Director/C&S.

4. A. K. Goswami, Director/TPL.

CLW:

S/Shri

1. R. K. Tewari, CEE/LOCO.

2. Vipin Kumar, Dy.CEE.

N. Railway:

S/Shri

1. Sunil Goyal, CEE.

2. R. K. Saxena, CELE.

3. Deepak Gerwal, Sr. DEE/TRS/GZB.

4. Anurag Agarwal, Sr. DEE/TRS/LDH

C. Railway:

S/Shri

1. R. K. Tiwari, CELE.

2. Sanjay Kumar, Sr. DEE/TRS/KYN.

E. Railway:

S/Shri

1. Gunanand Jha, CELE.

2. S. K. Chatterjee, DEE/TRS/HWH.

E. C. Railway:

S/Shri

1. A. K. Chattopadhyay, CELE.

2. Santosh Kumar, Sr. DEE/TRS/GMO

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N. C. Railway:

S/Shri

1. Anupam Singhal, CELE.

2. A. K. Gupta, Sr. DEE/TRS/CNB.

S. E. Railway:

Shri Kishore Kumar, CELE.

S. Railway:

S/Shri

1. Arun Kumar, CELE.

2. S. K. Natrajan, Sr.DEE/TRS/RPM.

S. C. Railway:

S/Shri

1. A. A. Phadke, CELE.

2. P. B. S. Rathore, Sr. DEE/TRS/BZA.

S.E.C. Railway:

S/Shri

1. S. N. Dubey, CELE.

2. B. K. Patel, ADEE/TRS/BIA.

W. Railway:

S/Shri

1. S. N. Singh, CELE.

2. Dinesh Jain, Sr. DEE/TRS/BRC.

W. C. Railway:

S/Shri

1. R. K. Mishra, CELE.

2. S. P. Singh, Sr. DEE/TRS/TKD.

E. Coast Railway:

Shri Kalyan Pattnaik, Dy. CEE/HQ.

IRIEEN

Shri Arun Dharmik, PROF./Loco.

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INDEX

SN ITEMS Proposed

by

Page

Nos

Inaugural Session 5-6

Technical Session- Part I (New Items)

1 Review of major schedule & TI schedule of conventional locos. NR 7-8

2 Review setting of Relay Q20 at 750 volt instead of 865 volt for

conventional Electric Locomotives.

ECR 9-14

3 Modification of cooling fan in SIV. SR, NR & SCR 15-21

4 Servomotor mounting base cover getting cracked due to less support wall

present near the molded insert provided in the base of the cover in

contactors 8.1 and 8.2.

WCR 22-24

5 Modification of CBC operating handle. SR 25-27

6 Modification to avoid Melting of Roof Bar (knife portion) in WAG-7

locomotive.

ECoR, NCR 28-30

7 Provision of rear loco notch position indicator in leading loco in MU

consists.

SR 31-34

8 Modification in brake pull rod pin in WAP-7 locos. SCR 35-37

9 Removal of Anti Spin valves in 3 phase locos. SCR 38-39

10 Standardization of various Speed Sensors provided in 3-phase locos. SER 40-41

11 Breakage of Push Pull Rod in WAP7 and schedule of replacement during

IOH/POH.

RDSO 42

12 Issues related with Vigilance Control device. RDSO, WCR 43-46

13 Modification to improve intensity level of Twin beam Headlight for

Conventional Electric locomotives.

ECR 47-51

14 Problems in radial interference on DE bearing seat of 6FRA6068 Traction

Motor.

CR 52-55

15 Provision of LED type light for exchanging signals with train passing staff. NR 56-57

16 Introduction of ‘H’ type tight lock coupler with Soft Draft Gear. Railway Board 58

17 Use of Composite Brake Blocks. Railway Board 59-60

18 RDSO & CLW jointly give presentation on status of reliability

improvement measures taken for IGBT propulsion.

Railway Board

RDSO

61-65

19 Presentation by SE Railway on benefits of using WAG9 MU in place of

WAG7 MU.

Railway Board

SER

66-67

20 Improvement in adhesion of WAG9 locos by providing additional sanders

and increasing efficiency of sanding operation.

Railway Board 68-70

21 “Procurement of spares from OEMs- Implementation of life cycle concept

to obtain reasonable prices and long term support from OEMs”.

Railway Board

SCR

71

Part II (Discussion on Status/Compliance on Decision on Items of 36th MSG

(Elect Loco) Meeting held at IRIEEN, Nasik Road on 21st & 22nd Nov’ 2013)

72-75

Concluding Session 76

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INAUGURAL SESSION

CEE/NR Address:

1. There is an urgent need to improve the reliability of three phase Locomotive.

2. As the Loco holding is increasing, the arising of POH would be more in time to

come, therefore, the construction of POH Shop at BRC should be expedited.

3. Best course of action for maintenance of Loco would be outsourcing of the

identified activities.

4. Variety of equipment in Loco should be avoided to ensure the ease of

maintenance and inter changeability.

5. Running of overdue Loco for schedule inspection should be monitored and

eliminated.

EDSE (Co-ord) Address:

1. Zonal Railways have given several useful suggestions/ideas for 37th

MSG

meeting. Out of these, 21 items proposed by Zonal Railways/RDSO/Railway

Board have been included in Agenda for discussions.

2. Remaining 45 items which could not be included are under further

study/examination. Action on all these items would be taken by RDSO in

consultation with zonal railways.

3. MSG have played an important role in improving the reliability of Loco since its

first meeting in Oct. 1968 when Electric Loco holding was around 500 and

electrified route was limited to around 3300 kms. MSG meeting provides a forum

for close interaction/discussion and suitable decision for reliability improvement.

4. Report for mid-term rehabilitation of three phase locos are under finalization.

Replacement of GTO converter with IGBT shall be planned during mid-term

rehabilitation of GTO converter locos.

Advisor (RS) /Address:

1. SPAD cases have increased in certain Railways. It must be reduced by intensive

monitoring/counseling of the crew.

2. Maintenance staff should be trained in a systematic manner to ensure that

technology of 3-phase Loco is imbibed smoothly for better/correct maintenance

practices.

3. Mid-term rehabilitation report for three phase Loco should be finalized by RDSO

early.

AML’s Address:

1. RDSO and CLW should work together to improve the reliability of Electric Locos

in consultation with Zonal Railways. Since loading target has been fixed at 1100

MT, the reliability of Electric locos is very important to achieve this target.

2. Performance of certain sheds like ELS/TATA, ANGL, BKSC, ASN, KYN, HWH

& TKD have deteriorated. This needs immediate improvement. There had been fire

in ELS/MGS based loco which is serious setback to fire safety. Efforts should be

made to eliminate fire incidences in electric locos.

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3. Similarly SPAD cases are a cause for serious concern for safety of train operation.

4. Since manufacturing of conventional locos are being stopped, the future is WAG-

9, WAP-7 & WAP-5 locos only. Therefore, reliability of the locos should be

improved

5. CRS sanction for multiple WAP-5 for mail, express working should be expedited.

ML’s Address:

1. MSG meeting is an important forum to discuss reliability issues. Therefore, it

should be regularly held every year. The performance of electric locos had not

been satisfactory during last few months. The ideas for improvement in reliability

should come from the sheds also.

2. Last GTO converter loco and last convention tap changer loco would be flagged

off this year by Sept/Oct.2015. It had taken about two decades to switch over

from conventional tap changer loco to 3-phase loco which is really very slow for

adopting new technology for reliability improvement.

3. Reliability and safety aspects of electric locos are of highest priority; therefore we

should make an all out efforts to avoid mid-section failures of electric locos.

4. Dead movement of locos should be avoided. Defective locos should be attended

in nearest sheds to the extent possible. Overdue running of locos has still not

improved. This should be watched/monitored at HQ as well as division level

closely so that locos are sent to shed in time. This will go a long way to improve

reliability of locos.

5. Fire safety is a major concern. Recent fire case in a loco of ELS/MGS shed should

be analyzed and steps must be taken to eliminate fire cases in locos.

6. Specific Energy Consumption (SEC) in some Zonal Railways like ECR, ECOR,

SR and SER have deteriorated. A detailed analysis should be made and action

should be taken to arrest the deteriorating trend. Effective ways and means should

be found out to monitor the SEC through Crew Management System (CMS).

7. Methodology for provision of Distributed Power Wireless Control System

(DPWCS) in electric locos should be chalked out so that it can be used more

fruitfully for freight train operation.

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TECHNICAL SESSION

Part-I

New Item

Item no. : 1

Subject : Review of major schedule & TI schedule of conventional

locos.

Proposed by : NR

File no. : EL/3.6.1/1 & EL/3.6.1

Note of proposing Railway:

At present the periodicity of AOH & TI schedule of freight conventional locos is 1.5 year

+/-10 days and 20 days respectively. The periodicity of minor schedule of conventional freight

locos had already been revised to 60 days (IA), 120 days (IB) and 180 days (IC) vide RDSO

letter no EL/3.6.1 dated 25.04.11.

As on date holding of shed has reached up to 200 locos. Therefore, it is difficult to carry

out major schedule after 1.5 years due to staff constraint resulting into large number of freight

locos are working with overdue schedule. The issue of revising the major schedule has already

been advised vide this office letter no 230-Elect/TRS/79 dated 24.11.14 & 02.06.14. Therefore, it

is proposed that periodicity of major schedule of freight conventional locos may be enhanced

from 18 months to 24 months and TI schedule from 20 days to 30 days respectively.

RDSO’s Note:

RDSO had already initiated the process for revising the following schedules of

conventional freight locos (WAG7, WAG5H & WAG5TAOchi):

(i) Trip inspection schedules from existing 20 days to 30 days

(ii) Minor schedules (IA, IB & IC) from existing 45 days to 60 days

RDSO has also considered for revising the AOH periodicity of conventional freight locos

from existing 18 months to 24 months. CR, NR, SR, WR, ECoR, SECR and WCR have agreed

with proposal. Feedback is awaited from ER, NCR, & SCR in this regard.

AOH periodicity (18 months) for WAP 4 locos equipped with Hitachi TMs and Minor

schedules (45 days to 60 days) for conventional freight locos have yet not been finalized owing

to non submission of performance feedback from following Railways:

SN Type of locomotives Performance awaited from

Railways

1. WAP4 locomotive with Hitachi TMs for 18 months AOH

periodicity

ER, NCR, SCR & SECR

2. WAG7 locomotive for 60 days Minor Schedule ECoR, ER,NR,WCR &WR

3. WAG5H locomotive for 60 days Minor Schedule Feedback pending from all

Railways.

4. WAG5TAOchi locomotive for 60 days Minor Schedule Feedback pending from all

Railways except SECR.

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Group may discuss the item & accordingly decision may be taken for regularizing

the aforesaid revised maintenance schedules or otherwise.

Deliberations:

Zonal Railways expressed that reliability of rubber item needs to be improved, so that it

can last about two years. Similarly sources of Manganese liners need to be developed, so

that the quality material is easily available for the use.

RDSO pointed out that revised specification of the Nylatron bushes and sandwich

mounting have been issued. Zonal Railways should procure the material as per revised

specification to get better reliability.

Recommendations:

Group agreed for extending periodicity of 2 years for AOH of conventional freight

locomotives (WAG7 & WAG5) on trial basis. Name of present AOH schedule may be

modified as schedule ‘ID’ since it is not being done annually.

Similarly for POH following schedule should be followed.

Time (years)

Schedule

Therefore POH schedule of conventional freight locomotives may be done after 10 years

in place of 9 years as indicated above.

Board’s decision:

Accepted. Performance of rubber items, liner & carbon brushes to be critically monitored

by Zonal Railways & RDSO.

Name of present AOH schedule can be changed to Term Overhauling (TOH).

After Implementation of decision to increase overhauling periodicity from 18 to 24

months, close watch should be kept on all safety & reliability aspects & Railways should

give feedback to RDSO on quarterly basis.

2 2 2 2 2

TOH TOH TOH IOH POH

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New Item

Item no. : 2

Subject : Review setting of Relay Q20 at 750 volt instead of 865

volt for Conventional Electric locomotives.

Proposed by : ECR

File no. : EL/3.2.172

Note of proposing Railway:

Preamble:

ELS/MGS is maintaining 174 locomotives; out of these 67 locomotives are WAP4 type

coaching and 89 WAG7 type freight locomotives. Flashing in traction motors and isolation of

traction motors thereafter have been a great cause of concern, and has resulted in line failures, and

punctuality loss of mail/express trains, and further infectiveness of the locomotive at the

destinations.

It has been observed on line during run, whenever there is QOP drop in loco, it is the skill

of loco pilot, and how he is able to isolate the faulty Traction Motor on line. Many times it has

been observed that in the process of isolation of faulty motor, there is loss of punctuality, and

further reduction of the tractive effort results into further loss of run in case of heavy loads and

gradient sections. Wrong isolation of motor further aggravates the situation.

Problem experienced:

While there are many reasons for earth faults in power circuits and QOP dropping,

flashing of TM is the major one and quite often one traction motor gets isolated on line. Cause

wise TM failures of ELS/MGS for last two years have been given below:

S. N. Cause wise failure 2012-13 2013-14

HOLDING 348 378

1 Arc-horn flashing 28 18

2 Bearing seized 07 02

3 Arm. Earthed/open ckt/balancing piece dropped 05 03

4 Carbon pig tail out/uprooted 11 06

5 “V” cone punctured 05 02

6 Ventilation net broken/Evolute coil

burnt/damaged

03 05

7 BBCR 03 07

8 Brush box spring broken 03 06

9 Misc. 02 13

Total 67 62

FRPCPY 19.3 16.4

% contribution of Arc horn flashing 41.8% 29.03%

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It is evident that cases of arc horn flashing contribute major part in the TM failures as

above last 02 years data have been taken, the Arc horn flashing cases have contributed 30 – 40 %

of failures in cases of TM isolation/failures.

Reasons for arc horn flashings:

Investigations have been carried out by sheds to find out reasons for arc horn flashing

and reduction of these cases which is causing adverse effect on the reliability.

It may be understood that there is a surge discharge through arc horn which protects

armature windings from outside surges in form of voltages, currents or power.

In case of less air gaps with the earth potential at arc horn, the surges tends to discharge

early, a standard setting of 11-12mm has been given as per manuals.

Over voltages of TM are limited by the arc horns, as higher voltages are discharges

through air gap.

As above discussed the arc horns are sort of protective devices for TM, proper settings of

air gaps are part of maintenance practices, but even in case of healthy practices arc horn flashing

occurs which affect the performance of TM and further repercussions as described above.

Analysis:

ELS MGS have worked in details for ascertaining the cause of arc horn flashing, various

data have been collected in these cases whenever TM has experienced flashover and loco has

failed or gone under repair. The Voltages, currents, notch position, shunting notch positions and

other environmental data has been collected from MPCS in the MPCS provided locos. The

sample data in 15 cases are given below which has been taken starting from Jan’14 to Oct’14:

DATA OF TM FLASHING CASES WITH ARC HORN FLASHING

S. No.

Dt. of failure

Loco No Position of flashed TM

TM voltage

TM currents Notch Shunting position

Power drawn by TM (KW)

1 18.01.14 22803 3 702V

TM1-842A, TM2-857A, TM3-

941A, TM4-811A, TM5-926A,

TM6-894A 28 4 660.58

2 15.01.14 22207 1 775V

TM1-910A, TM2- 920A,

TM3-736A, TM4- 814A,

TM5-873A, TM6- 897A 28 3 570.40

3 15.01.15 22207 3 632V

TM1-1176A, TM2-1169A,

TM3- 968A, TM4-1048A,

TM5-1098A, TM6-1151A 27 4 611.78

4 05.03.14 22907 6 754V 822A 27 3 619.79

5 06.05.14 22827 2 536V

(1) 1240 A (2) 1100 A (3)

1070A (4) 910A (5) 1200A (6)

1370 A 31 0 589.60

6 17.05.14 22798 5 764 V

(1) 300 A (2) 300 A (3) 310A

(4) 100 A (5) 340 A (6) 530 A 28 4

259.76

7 17.05.15 22798 6 404.92

8 10.06.14 22711 5 735 V (1) 389A (2) 403A (3) 416A (4) 379A (5)418A (6) 382A

25 0 307.23

9 10.06.15 22711 6 735 V 280.77

10 17.09.14 22824 559 V (1) 250A (2) 180A (3) 260A

TM 4, 5 & 6 N/A 24 0 145.34

11 19.09.14 22968 1 628 V (1)178A (2)353A (3) 460A (4)543A (5)493A (6)452A

22 2 111.78

12 04.10.14 22815 4 682 V (1)1312A (2) 1336A

(3)1318A (4)1285A (5)1161A (6) 1275A

27 0 876.37

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13 21.10.14 22710 5 688V (1)707A (2) 725A (3)697A (4)642A (5)777A (6) 769A

25 4 534.58

14 25.10.14 22804 1 602 (1)535A (2) 610A (3)627A (4)742A (5)675A (6) N/A

28 0 322.07

15 25.10.15 22804 2 602 367.22

Technical details of TM:

Before analyzing the above data, we must focus on the technical details of TM, as TMs of

different make are identical, ratings of CLW make Hitachi TM are reproduced below with the

reference of CLW manual for WAP1 as attached in Annexure-I:

Observations from data:

As the above data is analyzed, it seems that there have been varying voltages at the

time of flashing which have been below 800V. However in almost 50% of the cases

current have been high.

Further noticed that out of 15 sample cases, in 2 case the power drawn by the motor is

above the continuous rated power input into TM and in 5 cases the power input into

motor have been near and above 90% of the continuous rated power input of 630kW.

It can be concluded from the above data that the traction motor have been at higher

input power in the almost 50% of the case which have resulted the arc horn flashing

inside the motors.

Since the arc horns are primarily for limiting the voltages across air gaps by

discharging the extra energy through arcs, in all the cases the power drawn have been

high instead of voltages, had it not been the discharges, the voltages would have gone

at higher levels which could have cause further damages.

Therefore as discussed above ELS/MGS has view that limiting the voltages at the

motor terminal may control and reduce the arc horn flashing cases of TM.

Corrective measures and experiments by ELS/MGS:

Q20 Relay settings:

For prevention of TM from over voltage, Q20 relay is provided in the power circuit of

loco, the settings of this relay have been defined in the maintenance manual of CLW (attached as

annexure-II), which are being reproduced below:

Pick up 865V

Drop out 740V

The nominal voltage ratings of TM have been mentioned as 750 V, whereas the Q20

settings recommended as per manuals are 865V which is far above the ratings. Having setting at

such high level it seems Q20 was not able to prevent TM from over voltage.

Further RDSO has not issued guidelines till now regarding settings of Q20, however it

.cannot be denied that different zonal railways have been following the reduced settings of Q20

which are in practice.

Make CLW

Type HS 15250A

Continuous out put 630KW

Volts 750V

Starting Current 1350A

Continuous current 900A

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Experiments:

Upon further investigation & guidance provided by CELE/ECR, it was suspected that

higher Q20 setting of 865V (whereas nominal TM voltage rating is 750V) may not be preventing

from over voltages resulting in Arc-horn flashing cases.

As on experimental basis ELS/MGS has reduced the settings of Q20 to 750V, which is at

par with the continuous voltage rating of traction motors and have found encouraging results

which are produced below:

It was found that flashing cases of TM has been reduced. Comparative quarterly figures

of TM flashing cases shows that after modification started from 09.04.14 i.e. changes made in

setting of relay Q20 has causes reduction in flashing cases.

Suggestions:

From the above investigation, analysis and further the experimental data shows, the

flashing cases have drastically reduced after reducing the setting of Q20, therefore it is suggested

that the setting of Q20 needs to be revised to continuous rated voltage of TM i.e 750V instead of

865 volt.

While ELS/MGS suggests for review the settings of Q20 in order to reduce that arc horn

flashing case and in turn reduction of TM failures, following point are depicted to be discussed

further:

As the data shown the flashing cases has the relations with surge in the power or

heavier power drawn by the motors, although voltages are not appearing to be high,

there are inherent higher voltages induced in the TM which does cause the arc horn

flashing.

The results achieved after reduction of the setting have very encouraging as described

above, which indicates while clamping the voltages at the limit of its continuous

rating will limit the surges and higher power input and therefore does reduce the

chances of flashing.

The recommended setting of 865V as per manuals against continuous voltage ratings

of 750V appears inconsistent, as the voltages are never reaching at that level and Q20

remains dysfunctional, even at lower levels TMs are overpowered and flashing

occurs. Therefore review of setting is required.

In the past 2 to 3 years there have been increasing trends of loadings and speed both

which has resulted overpowering of TM, and thus the flashing cases have now been

significant. Therefore to protect the TM the review of setting is required.

While reducing the Q20 setting, operational requirement also need to be addressed,

ELS/MGS has been watching the performance of modified setting, there may be

chances for the loco pilot booking as “speed not pickup” or “Q20-pickup at lower

voltages”.

ELS/MGS has reduced the setting in 53 WAP4 locos, and has been watching the

performances, till now in the period of 3 quarters only 3 cases have been reported as

above, on investigation in all three cases the Q20 setting have been found disturbed

and reduced to 600-650V.

No such cases have been reported till now at the Q20 setting of 750V, however

performance is being monitored.

Period No of WAP4 locos with Q20 setting of 865V

No of flashing cases

% flashing cases

No of WAP4 locos with Q20 setting of 750V

No of flashing cases

% flashing cases

Jan’ 13 to Mar’13 58 09 15.5 Nil - -

Apr’ 13 to May’13 58 05 8.6 Nil - -

Jun’13 to Aug’13 62 05 8.1 Nil - -

Jan’14 to Mar‘14 55 08 14.5 8 Nil Nil

Apr ’14 to May’14 16 02 12.5 47 Nil Nil

Jun’14 to Aug’14 15 02 13.3 52 01 1.9

Sept’14 to Oct’14 14 02 14.3 53 01 1.9

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Material required: Nil.

In view of above, It is requested to consider the issue for 37th MSG discussion so that

setting of Q20 relay may kindly be reviewed, in order to prevent the TM from Arc-horn flashing

Relay Q20 need to be set at 750V(pick up) & 625V(drop out).

RDSO’s Note:

1.0 The different ratings defined in CLW specification no- 4T CLW/TM/Hitachi-15250A, for

traction motor type HS 15250A is as below.

Continuous rating: 750V, 900A, 630 KW

One Hour rating: 750V, 960A, 670 KW

5 min rating: 1300A

2.0 Test results of Commutation test with Direct and pulsating current carried out on original

Hitachi traction motor at M/s Hitachi Japan is given as under.

Table-1: Commutation test with direct Current:

Field

(%)

Voltage

(V)

Current

(A)

Field

Current

(A)

Speed

(rpm)

Commutation (Leading edge/ trailing edge)

CW CCW CW CCW

95

900 900 855 1102 1096 1/1 1/1

900 1350 1283 965 958 1/1 1/1

900 500 475 1423 1414 1/1 2/1

900 275 261.3 2156* 2150* 1/1 1/1

1125 375 356.3 2140* 2129* 1/1 1/1

40

900 900 360 1806 1797 1/1 1/1

900 1350 540 1416 1406 1/1 1/1

900 1100 440 1593 1571 1/1 1/1

900 700 280 2147* 2129* 1/1 1/1

*At the maximum service speed

Table-2: Commutation test with Pulsating Current:

Field

(%)

Voltage

(V)

Current

(A)

Field

Current

(A)

Speed

(rpm)

Commutation (Leading edge/ trailing edge)

CW CCW CW CCW

95

885 275 261.3 2131 2123 1/1 1/2

885 310 295 1940 1927 1/1 1/2

850 650 618 1185 1174 1/1 1/1

825 900 855 1008 1001 1/1 1/1

825** 1350 1283 881 874 1/2-3 1/3

40

850 650 260 2175 2137 1/1~2 1/2~3

825 900 360 1657 1649 1/2 1/1

825** 1350 540 1280 1280 1/3 1/1

Note: i) ** For information only

ii) Increasing the number e.g. 1, 2, 3 -indicate inferior commutation

3.0 From the table-1: it can be seen that commutation test at direct current has been

carried out at 900V at different field and different current ratings and result of

commutation is satisfactory.

4.0 From the table-2; it can be seen that commutation test at pulsating current has

been carried out at 825 v at rated current of 900A. It is not done at 900V as in the

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case of direct current. From this fact it can be inferred that at pulsating current the

voltage of the Traction motor cannot be increased more than 825 V at rated

current of 900A without affecting the commutation quality. Increasing the voltage

will cause inferior commutation quality and finally may results in commutation

related failures e.g. commutator flashing, chipping off carbon brushes, arc horn

flashing etc.

The above commutation test results are test bed results under stationary

conditions. In actual running condition the quality of commutation also affected

by shock loadings as the train negotiates point crossing and rail joints and current

collection quality from pantograph etc.

5.0 Data provided by ECR for 15 cases of flashing, which indicate that in all cases

there have been varying voltages below 800V at the time of flashing.

6.0 Experiment done by ECR by reducing the setting of Q20 to 750 V in 53 WAP4

locomotives and reported no case of flashing on traction motors in the period of

3 quarters with modified setting of Q20 at 750 V .

7.0 Railway Board vide letter no 2007/Elect(TRS)/441/7 dated 11.02.2015 also

expressed concern on increase in Hitachi TM failure cases causing punctuality

loss of trains.

In view of the above, as proposed by ECR, the setting of the Q20 relay may be

accepted.

Deliberations:

The modification suggested by ECR was discussed. It was found that most of the

Railways have already reduced the setting of Q20 relay based on their experiences to avoid

flashing of traction motors.

Recommendations:

It has been decided to change the setting of Q20 relay to, Pick-up voltage 790 volts and

drop out voltage 700 volts.

Board’s decision:

Accepted.

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New Item

Item no. : 3

Subject : Modification of cooling fan in SIV.

Proposed by : SR, NR & SCR

File no. : EL/1.2.9.1

Note of proposing Railway: (SR)

(A) Problem Experienced:

Frequent failure of SIV cooling fan due to bearing housing getting oblong and bearing

fails, in turn cooling fan failure.

Suggestion:

Due to the frequent failure and poor reliability of cooling fans of SIV, ELS/ED taken the

initiative to provide new robust type motor in AAL &Siemens make SIVs.

1. Modification of Cooling fan in AAL make SIV:

750W capacity motor in place of existing 500W. Also, it is cheaper than original motor.

So far done in two locos and performance is satisfactory.

Comparison of existing and modified Cooling fan assembly- 1 Capacity 500 W, 415 V,

3 Phase, 0.96 A

750 W, 415 V

3 Phase, 1.0 A

Ingress Protection IP 54 IP55

2 RPM 2800 2800

3 Price Rs. 1,21027/- Rs. 14,000/-

4 Mounting Flange mounted Foot cum Flange mounted

5 Protection Thermistor MCB with interlock

6 Bearing 6002 2ZC3 6004 2ZC3

7 Air flow 4 to 7 m/s 4 to 7 m/s

Original fan

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Modified fan assembly

Advantage:

Robust arrangement.

Cheaper in cost (savings/loco = ` 1,07,027)

Higher capacity.

Less failure.

Easy Maintenance.

Material Required:

3Ph squirrel cage induction motor Frame 80,

0.75 kW/1 HP, Duty S1, Insulation class F

Adapter – 01 no.

Hub – 01 no.

Impellor – 01 no.

2. Modification of cooling fan in Siemens make SIV:

Problem Experienced:

Poor Reliability of SIEMENS make self cooling fan.

Cost of the motor is very high.

Reliability of the motor is not up to the mark as compared to its cost.

Overhauling of motor is very complicated. Only skilled staffs can do.

End shields & casings are made up of Aluminium which is getting worn out at

bearing housing and bearing failures takes place.

Suggestion:

ELS/ED modified cooling fan for Siemens make SIV using MVSI motor and has been

provided in loco no 22713 in August 2014. Performance is so far satisfactory. Since MVSI motor

has a proven design, this will help to improve the reliability of the cooling fan.

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Comparison of Features of existing and modified Cooling fan assembly

SN Parameters SIEMENS Existing SIV

FAN

Modified FAN

Capacity 1800 W, 415 V 2200 W, 415 V

Make SIEMENS M/S GTR RANJAN

Current 3 Phase, 2.1 Amps 3 Phase, 2.6 Amps

Ingress Protection IP 55 IP55

RPM 2800 2800

Price 2,25,055/- 25,000/-

Protection MCB with interlock MCB with interlock

Mounting Side mounted Side mounted with strong

vertical support to base.

Remarks Casing and bearing seat is

made up of Aluminium.

Casing, Both end shields &

bearing seating area made up of

cast iron.

Conventional 3 Phase aux

motor.

Air flow 9 to 14.56 m/sec 9 to 14.56 m/sec

Photographs:

Existing

Modified Cooling fan assembly

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Material Required:

2.2 kW/3 HP 2 pole MVSI/MVSL motor with H class insulation

12 mm base plate -02 nos.

U channel 50X100X50 mm- 02 nos.

Clamps-04 nos.

Advantage:

Existing blower casing and impeller is utilized so no reduction of output.

Meggering of self cooling fan can be done in schedules since fan is having terminal

box. By tripping the MCB, can be meggered.

Greasing of bearings in IC schedule can be done due to the introduction of grease

pipes.

(B) Note of proposing Railway: NR

Failures of cooling fan bearings of M/s AAL make static converters are quite high.

Keeping in view large nos. of failures of cooling fan in M/s AAL make SIVs, cooling of the SIV

unit was provided using MVSI blower of conventional locos. For this purpose, one additional

MVSI cooling fan was provided adjoining to SIV unit & cooling air was passed to the unit

through a separate duct.

After making this arrangement, air flow measurement at critical locations of SIV was

made and found as given below comprising with SIVs fitted with original cooling fans, which was

sent to RDSO vide NR letter no 230-Elect./TRS/32/1, dated: 15.10.14.

S

N

Loco

no.

Detail of

cooling

arrangement

Date of

fitment

Air flow

measurement

in new

modified

arrangement

Air flow

measurement

in existing

arrangement

Protection

details of

MVSI, if any

1 27848

Existing cooling

fan removed &

MVSI motor

fitted near

MVMT-2 and

its air outlet

connected with

duct of existing

blower fan by

cutting from

MVMT side

Sept’13

during

AOH

At top side

jali near duct

opening -5.5

M/s.

At right

side jali (BA

panel side) near

duct opening-3.2

M/s.

At left

side jali

(MVMT side)

near duct

opening 2.3 M/s.

At top side

jali near duct

opening -5.2

M/s.

At right side

jali (BA panel

side) near duct

opening- 2.8

M/s.

At left side

jali (MVMT

side) near duct

opening 2.2

M/s.

Directly 3-phase

supply

connected to

MVSI from sine

filter capacitor

of SIV. The

existing wires

for thermostat

shortened, as in

MVSI winding

there is no

provision of

thermostat like

in existing

blower fan

motor and

further tripping

of SIV through

MCU card in

case any

abnormality in

blower fan

motor.

2

27655

Oct’13

during AOH

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It is evident from above measured values that air flow has improved with MVSI as

compared to SIV cooling fan. Encouraged with above results, ELS/LDH has fitted MVSI in 02

locos, first was fitted in loco no. 27848 in Sep’ 2013 during AOH, which is working satisfactory.

Second unit has been provided in loco no. 27655 in Oct’ 2013 during AOH. No failure/

abnormality has been reported till date in these locos on SIV account.

Advantages of MVSI in place of cooling fan of SIV in M/s AAL make:

Cost of cooling fan is approx. Rs 107149/-, while cost of MVSI is approx. Rs 20000/-

MVSI is fitted outside the SIV; therefore bearing sound can be monitored easily.

MVSI motor is easily available in sheds, so it can be changed in any shed.

In case of seat worn out of cooling fan bearing, it cannot be repaired. Similarly in case of

burning of cooling fan, rewinding is not possible. But maintenance of MVSI is well

established.

(C) Note of proposing Railway: SCR

Problems:

There are many loco failures on account of failure of SIV due to failure of its blower

motor in AAL make SIVs since insertion of SIV. Majority of blower motor failures are due to

bearing failure due to improper design of housing and bearing size and few cases are of winding

failures. As per RDSO reliability action plan bearings are being replaced after 18 months of

service. Even after periodical replacement of bearings, defects were noticed prematurely in these

motors. Further the cost of SIV blower motor is high leading to high maintenance cost of SIV on

account of blower motor. Due to these problems with SIV blower, some sheds are replaced the

SIV blower motor with MVSI motor (blower for Rectifier unit) provided in conventional

locomotives. However, the rating of MVSI is very high (3HP) compare to SIV blower (0.5 HP).

The rating of SCMRB is 1HP and with 2840 RPM which is nearer to the rating of SIV blower

motor (0.5 HP, 2750 RPM). The cost of the SCMRB motor is also very less compare to the cost

of SIV blower. Hence it is suggested to replace the AAL make SIV blower motor with SCMRB

motor.

Modifications:

SIV blower motor to be replaced with SCMRB motor by providing the same impeller of

SIV blower. To do this modification, shaft hub suitable for existing blower impeller to be coupled

to SCMRB and fixing plate similar to existing blower has to be fixed. Further, the churning fan

transformer may be shifted to convenient position for ease of maintenance.

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Material required:

01 HP motor-01 no, Shaft hub suitable for existing blower impeller- 01 no, Round fixing

plate (3mm thick/360mm diameter)- 01 no, L shaped flat to support transformer (8"/8")-02no, MS

plate (6"/8")- 02 Nos. Terminal SB- 01 no, Angular support for SCM RB- 02 nos.

Material rendered surplus: 0.5HP blower motor

RDSO Notes:

In view of high failure trend of cooling fan in 180 KVA SIV supplied by M/s. AAL,

sheds have carried out in house modification in few units as summarized below:

1. By providing of additional MVSI blower and connected SIV directly or through

canopy (NR).

2. Separate motor (750W capacity) with coupling arrangement of original impeller

motor in place of existing 500W (SR).

3. Provision of SCMRB motor (1.0 HP) in place of SIV Blower motor (SCR)

In this connection it may be noted that M/s. AAL has already introduced modified design

cooling fan with motor-impeller design & higher size bearing in new units. There is an addition

support at bottom in the modified design. Modified design has been cut-in from serial no

OB1801211022 from Oct’2012 onwards and total 117 units fitted with modified design of cooling

fan have been supplied by M/s AAL and out of 117 units, 91 units have already been

commissioned. Though the service period of modified units is less (around 1.5 yrs.) but it is

expected that modified design being in line with other makes will address the failures of bearing.

Modified design cooling fan with motor-impeller design

RDSO vide letter no EL/1.2.9.1 dated 23.06.2014 requested Railways to send the

performance of modified design cooling fan with motor-impeller design & higher size bearing.

The performance of modified design cooling fan with motor-impeller design has been received

from SER, ECR, WCR, and NR. No failures of modified design have been reported so far by

aforesaid Railways. The performance details are still awaited from SCR, CR, ECoR, SECR, SR &

WR. Railways to submit the field performance of modified design.

In this arrangement there is provision of thermal sensing as in the original design of

cooling fan, which provides protection against overheating of cooling fan winding. Firm has also

provided cooling fan KIT consisting of 26 items (accessories items for modification of cooling

fan). Firm has provided mounting stool for support of motor and also provided higher diameter

plate for fitment of motor. The new design fan can be provided in converter in serial no

OB1801008016 (year 2010 onwards) without any chassis modification and converter serial no

OB1800011001 to OB1801008015 needs minor chassis modification wherein input plate is to

provide on the side wall of panel.

In view of above, it is recommended that:

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(a) Railways may procure kit consisting of blower fan of modified design along with

accessories for its mounting (Kit consisting of total 26 items) in place of blower fan of old

design, as a spare part requirement (part number of modified design fan along with kit is

HHIM1801858) and released fan of old design are to be utilized by sheds as unit exchange

spares.

(b) Railways may carry out modification of cooling fan by provision of MVSI/ SCMRB

motor/Separate motor with proper mounting arrangement in 10 (ten) units each and submit

complete details along with performance report to RDSO for further study.

Deliberations:

SCR informed that they have provided M/s Havels make motor with impeller in M/s AAL

make SIV in place of cooling fan. SCR has further informed that there is provision of

thermal sensing in the alternate arrangement of motor-impeller design of blower fan.

ECoR informed that they have provided M/s Kirloskar make motor with impeller in 30

units of M/s AAL make SIV.

RDSO informed that M/s. AAL has already introduced modified design cooling fan with

motor-impeller design & higher size bearing in new units. There is an addition support at

bottom in the modified design. Modified design has been cut-in from serial no

OB1801211022 from Oct’2012 onwards and total 117 units fitted with modified design of

cooling fan have been supplied by M/s AAL.

Recommendations:

Railways to give feedback of modified design cooling fan with motor impeller

arrangement provided by M/s AAL to RDSO.

Railways may procure blower fan of modified design along with accessories for its

mounting in place of blower fan of old design, as a spare part requirement (part number of

modified design fan along with kit is HHIM1801858) and released fan of old design are

to be utilized by sheds as unit exchange spares.

SCR & ECoR to monitor the performance of M/s Havels and M/s Kirloskar make motor

respectively for further period of 6 months and give feedback to RDSO. Based on

feedback of above Railways, RDSO to issue modification sheet.

Board’s decision:

No of Railways like NR, SR, SCR & ECoR have tried alternate cooling arrangements for

SIV.As number of trials are already done, RDSO should collect the details & advise other

Railways also using such schemes in limited manner for all makes of SIV.

RDSO should consolidate the performance of all users and evaluate the reliability & cost

effectiveness of different cooling arrangements before issuing final instructions in the

matter.

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New Item

Item no. : 4

Subject : Servomotor mounting base cover getting cracked

due to less support wall present near the molded

insert provided in the base of the cover in contactors

8.1 and 8.2.

Proposed by : WCR

File no. : EL/3.1.35/2 (Elect)

Note of proposing Railway:

Problem:

Servomotor mounting base cover getting cracked due to less support wall present near the

molded insert provided in the base of the cover in contactors 8.1 and 8.2.

Investigation & Observation:

1) There have been 9 failures during 2013-14 & 7 during 2014-15 (up to

September). Average life is 4-5 yrs.

2) During tightening the moulded inserts become slacked due to less support wall.

3) On Further checking the SR contactor that is having the same servomotor

assembly. But in order to hold the servomotor assembly through hole

arrangement is provided in base cover and finally sleeves are provided at bottom

cross bar.

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Solution: Design philosophy adopted as of SR contactor.

Comparison of old and modified design in FB contactor

Cover having removed moulded insert and cross bar with modified sleeve (After

Modification)

Modified arrangement of contactor

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Status:

This arrangement has been provided in 7 locomotives, so far, and working satisfactorily

since September, 2013.

RDSO’s Note:

This may be taken up with supplier for modification in new designs and for existing

designs, RDSO will issue modification sheet.

Deliberations:

Group opined that such type of problems have not been experience by other Railways.

Railways brought out that since contactor are of Secheron make, hence it is not desirable to carry

out any alteration in the basic design of OEM.

Recommendations:

Item may be dropped.

Board’s decision:

Accepted.

SR Contactor Filter Contactor

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New Item

Item No : 5

Subject : Modification of CBC operating handle.

Proposed By : SR

File no. : EL/3.2.119/CBC

Note of proposing Railway:

Problem Experienced:

Frequent damage of CBC operating handle due to external hit.

Unable to open and close CBC due to bend of operating handles after CRO.

Excessive consumption of operating handles. In a year around 450 numbers of operating

handles have been changed.

Can be operated from one side only.

Deployment of manpower for changing the operating handle.

Suggestion:

Location change of CBC operating rod from bottom to top avoids deformation during

CRO. A drawing developed by ELS/ED in this regard in line with modification sheet issued by

Motive Power directorate of RDSO for Diesel locomotives is enclosed herewith.

Photographs:

Un-modified Modified

COMPONENTS TO BE FABRICATED:

Top lifter hook Top lifter Link Top lifter hook riveted with connector

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CBC top lifter hook and connector

provided in LOCK

LHS handle

Middle handle

RHS handle

Advantage:

Damages of operating handle due to CRO can be avoided as it is provided above CBC.

CBC failures due to bend of operating handle can be avoided.

CBC can be opened from both sides.

Damage of operating handles will be minimum.

Deployment of man power will be reduced.

RDSO’s Note:

Cases of breakages of operating handle have been reported by Railways during CRO. MP

Directorate/RDSO has already carried out modification vide modification sheet no.

MP.MOD.LD.05.10.11 Rev. (00) dated 18.07.11, which is applicable for electric locomotives

also. RDSO recommends Railways to adopt the modification.

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Deliberations:

The modification has been accepted by the group because of its inherent advantage over

present arrangement and is to be followed for E type couplers provided on conventional

electric locomotives. It was pointed out that this arrangement cannot be provided in

WAP7, WAP5 and WAG9 locos due to space constraints. RDSO will study this aspect

and issue suitable instructions for the provision of modified CBC operating handle in

three phase locos titled with ‘E’ type couplers.

Recommendations:

RDSO to issue necessary instruction to Railways for provision of modified CBC

operating handle.

Locomotives provided with ‘H’ type couplers will not need this modification.

Board’s decision:

Accepted.

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New Item

Item no. : 6

Subject : Modification to avoid Melting of Roof Bar (knife

portion) in WAG-7 locomotive.

Proposed by : ECoR & NCR

File no. : EL/2.2.21

Note of proposing Railway:

Loco-28467(WAG-7) was received from CLW and commissioned at ELS/ANGL on

21.07.2012. The said loco failed on line on 25.06.2014 in Khurda Division of ECoR due to knife

portion of one end of roof-bar no-5 melted inside U-clamp (connectors) and fell down on loco

roof.

Observations at ELS/ANGL:

The knife of roof-bar flashed and melted in the jaws of fixation U-clamp resulting knife

of roof-bar was broken and fell down on roof of loco.

The Lower bolt & nut assembly with compression spring used for tightness of fixation

jaws get rusted and the spring loses its stiffness completely (as shown in photo-2).

The upper locking spring arrangement of fixation jaws used to lock knife of roof-bar is

also having no stiffness and hard to operate and frequently broken.

Analysis:

Due to above reasons, the knife of roof-bar becomes loose in the jaws of fixation U-clamp

and vibrates during running of loco resulting into arcing between knife and jaws of U-clamp and

get melted particularly in rainy season get melted.

Thus, the existing arrangement for fixation of roof-bar is not suitable in WAG-7

locomotive & the modification is required to improve the loco reliability.

Roof bar melted &

touched hood

Rusted bolt, nut &

spring

Flash mark at the fixation jaw

of the roof bar knife

Existing Pull/Push type

locking arrangement in

Loco

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Modification by ELS/ANGL:

ELS/ANGL has provided nut & bolt type arrangement (M8 size) for ensuring proper

tightness & prevents any type of flashing due to vibration effects on the knife switch inside its

fixation U-clamp.

Materials required to carry out modification:

M8 nut & bolts (16 numbers per loco).

RDSO is requested for inclusion of the modification in 37th MSG agenda.

RDSO’s Note:

1. The existing arrangement of roof bar knife in the jaws of U-clamp has provision of bolt &

nut assembly with compression spring at lower side for ensuring tightness and locking

spring arrangement at upper side to ensure locking of knife of roof bar in fixation jaw.

These two arrangement need to be maintained properly to eliminate chances of vibrations.

2. Also, with the facts that majority of failure cases of roof bar flashing reported are

associated with ferrules side. Therefore, proposed nut & bolt assembly at upper side in

place of spring locking arrangement will not serve the purpose for reduction of roof bar

flashing cases experienced at ferrule side.

3. Railway Board vide their letter No. 2004/Elect/(TRS)/138/6 dt. 18.05.2005 have already

advised Zonal Railways that no modification is required to be done in roof bar and

existing arrangement should continue and same was also circulated by RDSO vide letter

No. EL/2.1.8 dt. 20.07.2005.

4. Further, RDSO vide letter no. EL/2.2.21 dt. 12.08.2010 has requested Railways to ensure

proper gap between roof bar knife blade and jaw, proper tightness of ferrule with

aluminium tube and proper tightness of check nut. The same should be ensured during

schedule maintenance.

5. From present statistics of roof bar flashing cases on conventional & 3-ph locomotives, it

is recommended to adopt roof bar assembly in conventional locomotives similar to 3-ph

locomotives. In this connection, CLW has already provided roof bar assembly similar to

3-Ph locomotive with some modification in two WAP4 locos [22914& 22926] and same

is working satisfactorily since last three years as reported by ELS/ET/WCR. The

approximate cost of this modification per locomotive is Rs.15000/- which is comparable

with roof bar assembly of 3-Ph locomotives. Hence, as a long term solution it is proposed

that same can be adopted during major schedule of conventional locomotives by Electric

Loco sheds/workshops.

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WAP4 (22914) provided with roof bar assembly of 3-Ph loco pattern

6. In view of above, it is recommended to adopt roof bar assembly in conventional

locomotives similar to 3-ph locomotives

Deliberations:

As the performance of roof bar arrangement as provided in three phase loco is

satisfactory, group agreed for modification proposed as existing in three phase

loco.

Recommendations:

Group recommended for provision of 3-phase type roof bar arrangement during POH

schedule to avoid such failures. Sheds may also adopt this modification during major

schedule.

RDSO should issue necessary modifications for its implementation.

Board’s decision:

Accepted.

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New Item

Item no. : 7

Subject : Provision of rear loco notch position indicator in leading

loco in MU consists.

Proposed by : SR

File no. : EL/4.2.15

Note of proposing Railway:

Problem Experienced:

Rail burning due to continuous wheel slip is a cause of concern in safety of the train

working. There are number of occasions this rail burning happened in multiple locos (MU)

particularly due to rear loco as there is no indication of notch position of rear loco for LPs.’

Background of Problem:

Multiple operations of locos are necessary to haul heavy loaded train for effective

utilization on saturated line. All WAG-5 locos are made multiple locos for hauling goods train.

The recent Railway Board’s instructions stated that single WAG5 locos are not permitted on line.

The problem being faced in multiple locos is mismatch of notch position though notch

synchronizing relay Q49 is provided. In quick regression, there is no synchronizing control and

hence notch between locos are became mismatch many times. There is no notch position

indication in driving cab for viewing rear loco notch position. The situation arise some time that

though leading loco GR is zero, rear loco may be in notch and this causes continuous wheel

rotating in rear loco resulted to rail burning. Specially this problem was noticed when the train is

stopped at the signals, the rear loco may be 3 or 4 notch and this causes wheel rotating at stand

still place causing rail burning. In order to avoid such incidences a simple device is developed to

know the rear loco notch position in leading driving cab.

Burnt rails

Modification Suggested:

Notch Position Indicator:

Conventional locos are fitted with Tap changer. This Tap Changer is on-load tap changer

and every step will have 100 movement and total 32 steps are there & total movement of tap

changer is 3200.

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The SMGR is having cam shaft which movement is in line with Tap changer movement.

The Angle Transmitter is fitted on the shaft which transmit signal to notch indicators provided in

both cabs to indicate notch position. This angle transmitter or Selsyn transmitter is requires 5

wires between transmitter and indicator. In multiple operations, the individual loco notch position

is displayed only in concerned locos since there is no jumper connection in Selsyn circuit.

Proposed System:

In addition to existing system, additionally a potentiometer is fixed in other 100 shaft of

SMGR. Potentiometer is one of the simplest form of angle transmitter. The shaft of potential

meter attached to the 100 movement per notch, the resistance value will vary depending upon

angle movement and there by voltage can be varied. This voltage can be read in leading loco

through the existing jumper as shown in the Fig.1.

Implementation of notch position indicator by using commutator arrangement:

The potential meter available in market is not suitable for continuous operation hence the

rugged design by using commutator & brush is planned as below.

The commutator having 36 segments and every 100 one segment will move and with PCB

attached fitted with resistance. The commutator is directly coupled with 100 notch shaft of SMGR

and every 100 movement one segment will shift causing varying output from 0 to 110V. Zero Volt

indicates 0 notch and 110 volts indicates 32nd notch.

The zero volt is representing zero notch and on first notch 25V will indicate and further

each notch 2.7V jump will be there up to maximum 32 notches by using suitable resistance. The

output voltage is taken through a diode which prevents accident damage during jumper testing or

emergency cross supply by any means. The spare BL interlock is used in service with voltmeter

so that only in working cab, the meter will indicate the rear loco notch position. It needs only one

jumper wire to indicate the rear loco notch position. The diagram is enclosed in Fig. 2.

This arrangement is provided in MU locos of ELS/AJJ 23378/ 23864 and working

successfully on line.

Remarks:

The above set up for each loco costs approximately Rs. 3,000/-. The above arrangement is

very simple. The issue of notch mismatch in MU locos is totally solved. The same arrangement

can be provided for both relay and MPCS type locos.

Diagrams:

Voltage will vary from 0 to 110V depends up on the angle of arm

Fig. 1

Potentiometer

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Photos:

RDSO’s Note:

1. RDSO has issued instruction for MU/consist operation in MPCS locos vide letter no.

EL/4.2.15 dated 22.08.2014 and 22.07.2013 for non-synchronization of notches. It

was advised to put MP on ‘0’ before braking to avoid such type of failures. If this

instruction is followed, no such failures will happen and no modification is required.

2. Problem of non-synchronization of notches will not come in MU locomotives

equipped with MPCS with revised specification no. ELRS/SPEC/MPC-FDS/0001

rev-3.

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3. The above proposed modification will work in ABB type ASMGR which is having

angle of 100

for one notch. But GANZ type ASMGR is having angle of 10.50 for one

notch, due to which it may not show actual notch position as in Ganz type ASMGR.

4. This modification may not work, when both the locomotives have different type of

ASMGR (say leading loco has ABB type and trailing loco has GANZ type).

5. Basic requirement is of giving indication to leading locomotive whether GR is zero or

not in trailing locomotive in MU operation. One way to achieve this is installation of

separate ‘LSGR Trailing Loco’ lamp with MU coupler wiring as shown below:

To B-

173T173

XX

YY

XX

YY

XX

YY

XX

YY

173T

173T

173

173

Cab-1

SBCab-2

SB

BD

BD

Inter communication MU operation for LSGR

Trailing locoLeading loco

LSGR-LL LSGR TL

To B-

173T173

XX

YY

XX

YY

XX

YY

XX

YY

173T

173T

173

173

Cab-1

SBCab-2

SB

BD

BD

LSGR-LL LSGR TL

6. In view of the above, Loco pilots should be counseled to put MP on ‘0’ before

breaking to avoid such type of failures and no modification is required.

Deliberations:

The issue was deliberated and it was decided to implement the decision of 36th

MSG meeting on multiple operation of tap-changer locomotives fitted with MPCS

and other reliability improvements measures taken in MPCS version 3.

The problem of non-synchronization of notches will not occur in MU locomotives

equipped with MPCS version 3.

The synchronization is not possible in MPCS Version 2.

Recommendations:

RDSO shall issue modification sheet separately to provide rear loco LSGR

indication in all the conventional tap changer electric locomotives

Board’s decision:

Accepted.

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New Item

Item no. : 8

Subject : Modification in brake pull rod pin in WAP-7 locos.

Proposed by : SCR

File no. : EL/3.1.35/2(Brake lever)

Note of proposing Railway:

Problems:

During safety drive it was observed large numbers of split pins for brake pull rod were

worn out at neck portion. There is threat of pull rod dropping, eventually obstructing the wheel

due to such wear and tear (Photograph -1). It is regular practice of removing these split pins in the

trip sheds for adjusting the loco brake power. In the due course, sometimes non standard split pin

may also get into the use which also becomes potential threat for pull rod dropping. To overcome

these eventualities, ELS/LGD proposed modification similar to WAP-4 having bolt with castle

nut and split pin.

Present arrangement:

Brake pull rod is fastened with brake hanger by roller pin of 28 x 80mm and split pin of

size10 x 63 (As shown in photographs).

Modifications:

Proposed arrangement:

Instead of roller pin with split pin, ELSLGD proposed to use M28 x 114mm Hex bolt

with plain washer, castle nut and split pin. (As shown in photographs)

Existing roller pin with head with split pin has to be replaced with M28 x 114mm Bolts.

Work to be carried out:

Existing roller pin with head with split pin has to be replaced with M28 x 114mm Bolts.

Applicability: All WAP-7.

Material required:

16 Nos of M28 x 114mm Hex head bolts (IRS-R-65) with washer, castle nut and split pin

of size 4 x 72mm per loco as per LGD Drg No. C/ELS/LGD/BOGIE/3/131.

Material rendered surplus:

16 Nos of roller pin with head of size 28 x 80mm and split pin 10 x 63 mm.

Ref: CEE/SCR lr.No.E.221/SMI/MD/TC/3Phase/Vol.IV dated 18.10.2014.

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Photographs

Condition of worn out split pins noticed during safety drive

Front view showing fastening of pullrod with cotter pin

and Hex.head bolt with castle nut and split pin

Rear view showing fastening of pullrod with cotterpin and

Hexhead bolt with castle nut and split pin

Zoomed view of modified and existing arrangement

Existing Proposed Photographs showing Existing and Proposed fastening of Pull rod in WAP7 brake rigging

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RDSO’s Note:

The arrangement proposed by SCR appears to be more reliable and RDSO

recommends to accept the modification.

Deliberations:

The modification has been accepted by the group on account of better safety.

Recommendations:

RDSO to issue necessary instruction to Railways.

Board’s decision:

Accepted.

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New Item

Item no. : 9

Subject : Removal of Anti Spin valves in 3 phase locos.

Proposed by : SCR

File no. : EL/3.2.19/3-Phase

Note of proposing Railway:

Problems:

In 3 phase locos Anti spin valves are provided to obtain a rapid but light brake application

to the driving wheels in case of wheel slip.

Subsequently it was decided to isolate the anti spin brakes, as per the Minutes of

performance review meeting of Three phase locomotives, issued by Railway Board vide

Lr.no.2001/Elec.(TRS)/440/18/7/Vol (II) 3phase dt:23.11.05. Accordingly the electric supply to

the EP valve has been disconnected. However, this valve is still being provided and connected in

pneumatic circuit as part of the brake system in new locos by CLW.

In some of the cases it is observed that leakage of MR is taking placing from this valve

due to damage of rubber gaskets and this valve either to be dummied or overhauled to arrest the

leakage. One additional double check valve is also provided to direct either the output of anti spin

valve or D2 direct (SA9) valve to brake cylinder. If the anti spin valve is dummied or removed

from locomotive, then the additional double check valve also can be removed from locomotive.

Benefits:

By removing anti spin valves and associated double check valves, annual savings of

approximately Rs.8 lacs can be achieved by a shed of 100 locos.

The cost of two nos. each of Anti spin valve and double check valve can be also saved, if

CLW does not provide in new locomotives at production stage itself.

Reduced requirement of man power for overhauling/attending these valves in case of air

leakage or overhaul at maintenance sheds.

Savings:

1. Cost of maintenance kit for anti spin valve = Rs.15,913/-

2. Cost of Maintenance kit for double check valve = Rs.2922/-

3. Population of anti spin valves in 100 locos= 100×2= 200 nos.

4. Population of Double check valves to be removed = 100×2= 200 nos.

5. Total saving in maintenance kits = 15913×200+2922×200 = 31,82,600 +5,84,400 =

Rs. 37,67,000/-

Since maintenance kit is being provided in every 4.5 yrs, annual saving per annum Per

100 locos would be Rs. 08,37,111/-

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Modifications:

As anti spin valves are already isolated electrically, it is proposed to remove anti spin

valve and associated double check valve from three phase locomotives.

RDSO’s Note:

1. RDSO has carried out trial in Dhanbad Division. During trail it has been noted that anti

slip Brakes are reducing the haulage performance of WAG-9 locomotive. Frequency of

occurrence of wheel slip is also nearly the same with and without ASB. Even if, anti-slip

brake is disabled, the wheel slip gets arrested automatically very quickly.

2. On the basis of above findings, it was recommended vide RDSO letter no. EL/3.1.35/2

dated 13.10.2005 to isolate ASB on WAG-9 and WAP-7 electric locomotives on trial

basis for a period of one year and user Railways were to monitor the performance of

locomotives so that a final decision could be taken.

3. South Central Railway has informed that even after power supply to anti spin valve is

disconnected there is leakage of MR due to damage of rubber gaskets.

4. The issue has been discussed in Reliability meeting held at CLW on 27/28.04.2015 and

consensus was expressed by all participating Railways on removal of anti spin valve in

three phase locomotives as indicated in para 4.7 of Minutes of Meeting issued by CLW

dated 18.05.2015.

In view of the above, it is suggested that in addition to cost saving, the removal of ASB

will increase the reliability of locomotives & it is recommended to be removed.

Deliberations:

Railways have agreed for removal of Anti spin valve along with its double check valve.

Recommendations:

CLW to modify the scope of supply given in the specification of brake system of 3-pahse

locomotives.

RDSO to issues modification sheet for removal of anti-spin valve and its double check

valve in the 3-phase locomotive already in service.

Board’s decision:

Accepted.

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New Item

Item no. : 10

Subject : Standardization of various Speed Sensors provided in 3-

phase locos.

Proposed by : SER

File no. : EL/3.1.35/26

Note of proposing Railway:

Speed sensors fitted in three phase loco are different from each other with respect to

coupler configuration even in similar make of speed sensor. More over literature and maintenance

manual is not also available to us. Therefore, it is very difficult for daily maintenance as well as to

the sheds to maintain spares of each type speed sensor.

Details of Make-wise speed sensor provided in 3-Phase loco and arising are furnished

below.

Make of Speed Sensor No. Of Coupler No. of Pin Population

(TATA shed)

Arising

(2013-14)

Arising

(2014-15)

M/s ARC in GTO loco 3 5, 5, 3 22 4 9

M/s ARC in IGBT loco 2 5, 5 7 0 3

2 5, 3 1 0 1

Lenord Bauer in IGBT

loco

1 8 5 0 1

2 5, 3 1 0 0

Jaquet Technology in

IGBT loco

2 5, 5 6 0 0

2 5, 3 2 0 0

M/s ARC (Dopler

Base) in IGBT loco 3 5, 5, 3 Not fitted

Laxven system in

IGBT loco 2 5, 3 1

0 0

Therefore, it is requested that RDSO may look into for Standardization of Speed sensor

with coupler pin and advice the firms accordingly. It also suggested that the item may be included

in the agenda for discussion in 37th MSG.

RDSO’s Note:

1. As per OEM design two five pin connectors was needed in Weigend sensors for double

channel. Further, one external power supply connector of three pin is needed for active

speed sensor of Hall Effect based of M/s ARC. Hence for ARC make sensors in GTO

based locomotives invariably three cables of 5, 5, and 3 pin connectors are needed.

2. For IGBT based converters as initially speed sensors were not standardized, hence BT has

used one cable with 8 pin connectors. M/s BHEL & M/s ABB have used two cables with

5, 5 connectors initially and thereafter CLW has standardized as two cables with 5 & 3

connectors.

3. Presently Lenord Bauer, Jaquet & Laxven make speed sensors are of two cables with 5 &

3 connectors.

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4. Railway can modify two cables 5, 5 pin connectors of ABB and BHEL with 5 & 3 pin

connectors provided in initial locos. The quantity may be approximately 30 locos.

5. It may be noted that M/s BT has used 200 teeth sensors and others have used 120 teeth

sensors. This needs to be stopped in further supply.

6. The speed sensors have now been standardized in specification of IGBT based traction

converter of CLW.

7. For existing systems, a level of standardization may be achieved by analyzing different

pin configurations.

Deliberations:

RDSO informed that two 5-pin circular connectors were needed in Weigend sensors.

During induction of active sensor, one circular connector for power supply was required,

hence active sensor of M/s ARC make in GTO based locomotives invariably has 3 cables

of 5, 5 & 3 pin connectors.

For IGBT locomotives, speed sensor were not standardized initially hence manufacturers

had adopted different configuration such as M/s BT has used one cable with 8 pin

connector and M/s BHEL and M/s ABB have used two cables with 5, 5 pin connectors

initially. These speed sensors (5, 5 pin connectors) were provided initially in

approximately 30 locos.

Subsequently CLW has standardized the configuration as two cables with 5 & 3 pins

connectors (Signal connector- 5 pin circular connector & power supply- 3 pin circular

connector).

Presently Lenord Bauer, Jaquet & Laxven make speed sensors are of two cables with 5 &

3 connectors.

The speed sensors have now been standardized in specification of IGBT based traction

converter of CLW. Speed sensor shall be supplied as per CLW specification No.

CLW/ES/03/0528 dated Nov’.12 or latest. Active speed Sensors with 120 tooth wheel

ring duly shall be provided.

Recommendations:

Manufacturers to supply speed sensor with 5 & 3 pin connectors and 120 tooth wheel ring

as specified in CLW’s specification.

Railway may modify two cables 5, 5 pin connectors provided initially (around 30 locos)

with 5 & 3 pin connectors.

RDSO should issue necessary guidelines/instructions in this regard.

Board’s decision:

Accepted.

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New Item

Item no. : 11

Subject : Breakage of Push Pull Rod in WAP7 and schedule of

replacement during IOH/POH.

Proposed by : RDSO

File no. : EL/3.1.35/12

Note of proposing Railway:

RDSO’s Note:

Railways have reported numbers of failures of traction link in WAP7 locomotives from

weld and base metal interface. RDSO/CLW has studied the problem and following action has

been taken/ recommended:

1. Radiography test of welding joint as per AS 1554.1-1991 has been introduced since

20.11.2012 as per CLW drawing no. 1209.01.113-006.

2. Groove angle for welding has been increased from 300 to 45

0.

3. Welding portion not to be machined.

4. M/s KMRI the OEM for this item has supplied push pull rod with the above modifications

from Sr. No. 680 onwards. No failure of these push pull rod has been reported by

Railways till date. As such, RDSO vide letter no. EL/3.1.35/12 dated 17.06.2015,

advised Railways that push pull rod in WAP-7 locomotives with serial no. prior to 680 i,e

679 or less needs to be replaced by new/modified push pull rod as per CLW drawing no.

(1209.01.113-006) or latest.

5. Present replacement schedule for traction link assembly is during POH (9 years for WAP-

7 /12 years for WAG-9), it is proposed that the replacement schedule should be changed

from POH to IOH to improve reliability.

Deliberations:

The breakage of push pull rod has been discussed and all failures of push pull rod are

prior to sr. no. 680 i.e. rod without radiography test.

RDSO presented the various modifications to be carried out by CLW to improve the

reliability of the product.

Use of forged flange of push pull rod instead of casted flange was also discussed.

Periodicity of change of push pull rod was also discussed in WAP7 locomotives.

Recommendations:

Railways to carry out instructions issued by RDSO vide letter no. EL/3.1.35/12 dated

17.06.2015.

CLW should incorporate changes recommended by RDSO regarding diameter of the tube

and angle in the drawing of the component.

RDSO to develop push pull rod with forged flange for 20 loco sets of WAP7 loco.

Push pull rod should be replaced during POH as a must change item.

Board’s decision:

Accepted.

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New Item

Item no. : 12

Subject : Issues related with Vigilance Control device.

Proposed by : RDSO, WCR

File no. : EL/3.1.14

Note of proposing Railway: (WCR)

Background:

Vigilance control device is fitted in loco to avoid the failures due to non alertness of loco

drivers, which check the alertness of driver with the some logical inputs by the driver actions

from working cab of loco. There are several issues related with VCD circuit, reliability and

standardization. All the issues have been clubbed together and taken as one item.

1. Modification in VCD circuit required: In present system, the power supply to VCD is available as soon as battery is switch on.

In multiple loco operations, battery is on in both locos. Due to this, supply will be available to

VCD main unit in both Locos, but BL key is ON only in leading loco. Now as Driver is in leading

loco, then supply ON/OFF of VCD main unit of trailing loco will not affect its alertness.

If there is malfunction in VCD main unit of trailing loco, this will de-energize the IP

valve and will cause BP pressure to drop. Accordingly brakes will be applied in both loco and

driver will not understand the cause for it as rear loco VCD is in suppressed mode, thus he won’t

able to identify and rectify it. This will cause undue failures.

In ET base multi loco 23109+23734, there was malfunction in VCD main unit of trailing

loco 23734. This caused extension of power supply to the QVCD and de-energization of the IP

valve and led to drop in BP pressure. Accordingly brakes applied in both loco and thus led to

failure as the reason for failure could not be ascertained at that time due to rear loco VCD

malfunctioning.

RDSO’s Comments: The circuit may be modified as suggested by WCR. Group may discuss.

2. Reliability of VCD: (Item proposed by SER & RDSO)

RDSO’s Note: A reliability meeting of VCD suppliers has been conducted at RDSO on 29-5-15 with

Zonal Railways and suppliers. In order to improve reliability there is a need to simplify the design

of VCD in line with VCD provided in diesel locomotives. A comparison of VCD of conventional

locos and diesel locos is enclosed.

There is a need to further modify VCD in line with stand alone VCD of diesel locos.

1. Acknowledgement from horn may be taken out as in three phase loco. This may improve

reliability due to defect in Horn pressure switch.

2. Low speed signal may also be removed and VCD suppression logic may be standardized

in all make.

3. The data logging may be rationalize by logging only essential events such as POWER

ON/POWER OFF/A9 OPERATED/SA9 OPERATED/ IP PROBLEM/QVCD RELAY

DEFECTIVE/VCD BYPASS BUT HEALTHY/VCD BYPASS AND FAULTY/VCD

FAULTY/VCD REACTIVATED/PB APPLIED shall only kept and events such as

NOTCH UP/NOTCH DOWN/FOOT SWITCH OPERATED/PUSH BUTTON

OPERATED/HORN OPERATED/SANDER OPERATED may not be recorded;

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Deliberations:

A. Modification in VCD circuit required (WCR):

The issues raised by WCR for modification in the VCD circuit to avoid mal-functioning

of VCD main unit of trailing locomotive has been deliberating during the meeting. Most

of the Railways informed that such type of problem have not been experienced by them.

Western Railway has pointed out that the modification proposed by WCR has already

been implemented in all locomotives of WR.

Comparison of features of VCDs of Conventional Tap Changer, Standalone Diesel and 3 Phase loco S.

No

Features Indications Conventional Tap changer

loco

Diesel Loco 3 Phase Loco

1. Vigilance cycle

Reset action

- MP/MPS-1/A-9/SA-

9/Horn/sander/paddle

Switch/Reset push button

Throttle handle/A-

9/SA-

9/Horn/sander/Reset

push button

MP/sander/paddle

Switch/Reset push

button/ A-9

2. Vigilance cycle T0 - 60+-2 sec 60 sec 60 sec

3. Warning Cycle

T1-level-1

Yellow

flashing light

8±2 sec 17 sec -

4. Warning Cycle

T2-level-2

Yellow

flashing light

and buzzer

8±2 sec 17 sec 8 sec

5. Penalty Brake Cycle

T3-level-1

32±2 sec yellow flashing with

buzzer

34 sec yellow flashing

only

120 sec yellow

flashing with buzzer

6. Penalty Brake Cycle

T4-level-2

Yellow

flashing light

with buzzer

Until reset continuous glow

with buzzer

Until reset No

indication No buzzer

Until reset

continuous glow

with buzzer

7. Vigilance

Suppression

- Yes, with A-9/SA-9/low speed

signal

with A-9/SA-9 only Yes, low speed

signal and A-9/SA-

9

8. Vigilance Bypass - Yes Yes Yes

9. Indications - On cab Unit:

Green :Healthy

Red: Bypass

Red flashing: faulty

Yellow flashing: Warning

cycle

On indicator Unit:

Blue :Healthy

Yellow: Bypass

Red: Penalty Brake

Yellow flashing:

Warning cycle

Green: MU mode

At Driver desk

panel A

Yellow lamp for

Vigilance Warning

10. Other features

11. Construction - 2 cab unit + 1 main unit 1 main unit+1

indicator cum reset

unit

Integrated with loco

brake system

12. LCD display - Yes No With loco display

13. Counter No Penalty brake counter

on main unit

No

14. Data Logging Yes with following

POWER ON

POWER OFF

FOOT SWITCH OPERATED

PUSH BUTTON OPERATED

A9 OPERATED/SA9

OPERATED /HORN

OPERATED/SANDER

OPERATED

NOTCH UP/NOTCH DOWN

IP PROBLEM/QVCD RELAY

DEFECTIVE/VCD BYPASS

BUT HEALTHY /VCD

BYPASS AND FAULTY

/VCD FAULTY/VCD

REACTIVATED

PB APPLIED/VCD

SUPPRESSED

No Data Logging No separate data

logging with loco

DDS.

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Group opined that though the problem has not been experienced by majority of sheds but

it is better to modify the circuit of VCD so that VCD gets 110 V power supply through

BL key interlock.

B. Simplification of VCD circuit (Proposed by RDSO):

Railways have agreed that the suggestion made by RDSO regarding de-activation of horn

signal for resetting of VCD may be accepted as it will improve the reliability due to

defects in horn presser switch.

RDSO pointed out that VCD remains in suppress mode in any of the following four

conditions:

i. Application of brake either through A-9/SA-9.

ii. Speed below to 2 KMPH.

iii. Manual control of GR.

iv. Working as a trail locomotive.

RDSO has proposed for removal of low speed signal for suppression of VCD as it is not

available in all locomotives.

Regarding removal of low speed signal for suppression of VCD, ECR and ECoR pointed

out that it will lead to unintentional application of penalty brake. Railways pointed out

that it takes few minutes for creation of BP pressure to 5 kg/cm2

and release of train

brakes and loco pilot takes notch only when BP pressure developed as 5 kg/cm2 .

Hence it

may lead to application of penalty brake before start of train if loco pilot fails to take any

action for resetting of VCD after releasing the brakes (A-9/SA-9). RDSO informed that

loco pilot has to be in vigilant mode once the brakes (A-9 or AS-9) are released.

The proposal for rationalization of data logging by recording only essential events has

been accepted by the group and data to be recorded/not to be recorded, as discussed

during the meeting are as follows:

Events to be recorded:

POWER ON/POWER OFF

A9 OPERATED/SA9 OPERATED

IP PROBLEM/QVCD RELAY DEFECTIVE

VCD BYPASS BUT HEALTHY

VCD BYPASS AND FAULTY

VCD FAULTY/VCD REACTIVATED

PB APPLIED

Events not to be recorded:

NOTCH UP/NOTCH DOWN

FOOT SWITCH OPERATED

PUSH BUTTON OPERATED

HORN OPERATED

SANDER OPERATED

Railways have agreed that the suggestions made by ELS/JHS/NCR for periodicity of

replacement of foot paddle switch, LEDs and buzzer, as given below, may be accepted.

ACK push button and LEDs in every AOH.

Buzzer, foot paddle switch and horn pressure switch in every IOH.

Recommendations:

RDSO to issue modification sheet for:

a. Provision of 110V battery supply to VCD through BL Key interlock.

b. Removal of horn signal for resetting of VCD.

RDSO to co-ordinate with VCD manufactures for modification of software for recording

of vital events only.

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RDSO to issue replacement periodicity of foot paddle switch, ACK push button, LEDs

and buzzer as deliberated during meeting.

RDSO to take feedback of Railways for removal of low speed signal.

Board’s decision:

Accepted.

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New Item

Item no. : 13

Subject : Modification to improve intensity level of Twin beam

Headlight for Conventional Electric locomotives.

Proposed by : ECR

File no. : EL/6.11.1

Note of proposing Railway:

Permeable:

Poor Head light intensity has been experienced by ELS/MGS since longer time, and has

been reported from various quarters from time to time, for example, LPs and ALPs have often

complained that headlight intensity has been poor in the log book. It has been reported also time

to time during foot plate inspection by officers and staff also especially in m/e trains. Further

there is a huge belt of foggy weather in the winter season across NCR and ECR, the volumes

reported have been high and has caused regulation of speed in the affected sections. Being related

to safety, it has caused wide attraction by other departments also. Safety department has advised

many times about improving safety, this is one area which needs to be improved.

ELS/MGS has stressed upon the requirement of proper headlight intensity and analyzed

the problem in depth in a following manner:

The illumination level at 8 meter should be ideally 4800 lux as per RDSO spec. No.

ELRS/Spec./PR/0024 Rev ‘1’ enclosed as Annexure-I and if the illumination level is

less than 4000 lux, shield reflector should be changed.

At ELS, MGS one cycle checking of intensity (lux level) of twin beam head light has

been started from 16.05.2013 during inspection and overhauling, till date exercise

worked out for 83 conventional electric locomotives. The sample datasheet is given

below:

Date Loco

No

DC to DC conv.

output voltage

LUX Lux after changing

bulb & Reflector

Cab1 Cab II Cab1 Cab II

24.07.13 21248 24.6 V 3100 3200 3200 3400

04.06.13 21346 25.5V 3000 3200 3300 3450

05.10.13 21382 25.25V 3100 3200 3300 3400

27.06.13 21391 25.4V 3000 3200 3300 3500

05.10.13 22588 25.8V 3100 3200 3250 3450

07.10.13 22739 25.85V 3000 3100 3300 3450

07.09.12 22815 25.7V 3000 3100 3400 3550

26.09.13 22860 25.5V 3100 3150 3300 3500

11.10.13 22861 25.6V 3000 3100 3300 3450

23.10.13 22868 25.6V 3000 3200 3250 3400

01.11.13 22869 24.9V 3100 3200 3300 3450

02.10.13 22906 25.6V 3100 3150 3300 3550

12.10.13 22937 25.6V 3000 3200 3250 3400

05.11.13 22946 25.8V 3100 3200 3300 3500

03.10.13 22947 25.5V 3200 3300 3400 3550

28.10.13 22955 25.65V 3100 3200 3400 3500

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09.11.13 22968 25.75V 3200 3300 3400 3550

04.10.13 22969 25.82V 3300 3200 3500 3700

26.10.13 22062 25.2V 3000 3200 3400 3600

24.10.13 22963 25.65V 3000 3100 3250 3400

25.07.13 22207 25.65V 3000 3100 3400 3600

03.11.13 27008 25.4V 3100 3300 3400 3600

18.10.13 27011 25.2V 3100 3300 3400 3600

12.10.13 27013 25.25V 3100 3300 3400 3550

22.10.13 27032 25.35V 3100 3300 3350 3600

31.7.13 27049 25.65V 3100 3300 3300 3500

17.06.13 27050 25.6V 3150 3300 3400 3600

30.08.13 27065 25.4V 3100 3250 3400 3600

27.9.13 28286 25.55V 3150 3200 3500 3650

15.9.13 28288 25.8V 3000 3200 3300 3500

08.8.13 28291 25.85V 3200 3400 3400 3550

06.10.13 28494 25.6V 3100 3200 3350 3600

26.10.13 28495 25.75V 3100 3200 3350 3550

11.9.13 28497 25.45V 3200 3300 3400 3700

23.12.13 27006 24.8V 3100 3300 3400 3600

01.01.14 27523 24.3V 2980 3200 3300 3500

9.1.14 21377 24.2V 3150 3300 3400 3550

23.1.14 27009 25.10 3150 3300 3350 3600

12.2.14 27022 24.8V 3100 3300 3450 3650

28.1.14 22909 25.0V 3200 3350 3400 3550

13.2.14 27042 25.5V 3100 3300 3400 3650

24.03.14 22588 25.4V 3250 3400 3350 3600

It has been observed that lux level of most of the locomotive’s head light is less than

3500 lumen instead of standard lux level value of 4800 Lumen. After replacement of

new shield reflector and bulb, there is only marginal increase in the lux level. Further

all efforts has been taken as per maintenance schedule, however the lux level has not

improved above 3500 in the above exercise.

Further, measurement of voltage level at various nodes was done starting from DC-

DC convertor upto head light terminal in both cabs. It was recorded as 24 Volt at

DC-DC converter terminal while at head light terminal on both ends recorded 02 to

04V less i.e. 20-22 volts. Indicative diagram is given below:

The line diagram of existing headlight circuit:

Further voltages at various nodes also indicated above shows that there is significant

reduction of voltage in the cables BD to SB cab1 as well as SB cab2.

DC to DC

converter

BD

SB

Cab2

23.30v

Cab2 HL

SB Cab1

Cab1 HL

Cable size 2.5 mm²

Cable size 2.5 mm²

23.30 V 22.54 V

24.52 V 23.82 V 22.73 V 20.35 V

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It is also required to mention here that BLPRD, BLPRF & BLPRR switches are rated

for 10A (AC). With adoption of DC-DC convertor for twin beam head light these

switches carry about 8-9A (DC) against DC rating of 6A only. This resulted voltage

drop across interlocks of these switches, value observed about 0.2-0.3 volt.

Following the above analysis ELS/MGS has observed that the voltages are dropping

across cables and the switches in the circuit and is being found 2-4 volts less at headlight

terminals, Corrective steps were taken as on experiment basis in order to find out any possibility

for enhancement of lux level as follows:

1 Replacing the three cables from DC-DC Converter to BD, BD to SB Cab1 and BD to

SB Cab-2 by higher sizes from 2.5sqmm to 10sqmm.

2 Replacing the two cables from 2.5 sq mm size by 4 sq mm between SB Cab-1 to H/L

Cab-1 and SB Cab-2 to H/L cab-2.

3 Replacing of the BL switches BLPRD, BLPRF & BLPRR by switches with two

parallel interlocks.

ELS/MGS has experienced some good results as voltage drops have reduced which has

lead to enhancement in the lux level of headlight. The same is further discussed ahead.

Modification suggested:

A trial have been done on experimental basis in five locos of ELS/MGS base by replacing

the 2.5 sq.mm size cables by 10 sq.mm among DC to DC convertor, BD and SB cab 1 & 2 while

cables of thickness size 2.5 sq.mm are replaced by 4 sq.mm between SB cab 1& 2 to Head light

terminals cab 1& 2. Voltage drops are minimized as results there is significant enhancement in the

lux level of head light. The indicative diagram for voltages is given below:

Intensity level of head light recorded after changing reflector & bulb with existing &

modified circuit in 04 locos parameters are appended below.

SN Loco

No.

Voltage

At DC-DC

output

terminals

Voltage (DC) volt at Head

light terminals

Intensity (in Lux)

measured in cab-1

%

improvem

ent in lux

level With

existing

circuit

With

modified

circuit

Stan

dard

value

With

existing

circuit

With

modified

circuit

Cab 1 Cab 2 Cab 1 Cab 2

1 22817 24.63 20.75 22.75 23.20 23.35

4800

3475 4062 16.89

2 22869 24.42 19.95 22.35 23.10 23.26 3409 4052 18.86

3 22870 24.51 20.25 22.51 23.16 23.30 3398 4030 18.59

4 22937 24.50 20.20 22.45 23.15 23.28 3397 4039 18.89

DC to DC converter

BD

SB

Cab2

24.50 V

Cab2 HL

SB Cab1

Cab1 HL

Cable size 10.0 mm²

Cable size

10.0 mm²

Cable size

4.0 mm²

24.50 V

23.35 V

23.20 V 24.50 V 24.50 V 24.50 V

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The Above experiment shows improvement in the lux levels of headlight by 500-600

lumens which are still well below the standard values.

Further as the voltages are dropping across the three BL switches in circuit, they are

replaced by the switches having 2 N/O interlocks and both are paralleled. This reduced the

voltages drop across the switches by 0.2 to 0.3V, and therefore will result further enhancement in

the lux level.

Therefore the above discussion and detailed analysis, the above modification is suggested

by ELS/MGS which will improve safety measures in the locomotives.

On detailed investigation and replacement of 2.5 mm² cable by 10 mm² cable from DC to

DC converter to BD panel & from BD panel to SB Cab1 & 2 and replacement of 2.5 mm² cable

by 04 mm² from both SB cab 1&2 to headlight terminals, the voltage level at headlight terminal

was recorded to be 23.2 volt in cab-1 & 23.35 in cab-2 and consequently the intensity improved

up to 4000-4100 lumen. This modification has been completed in 04 nos. locomotives and

intensity level is improved by 16-20%.

Further as the voltage drop across switch is considered. After parallelization it is expected

that lux level will further improve as there is reduction of voltage drop by 0.2 to 0.3 volt.

In view of above, it is thus established that thin size of cable and voltage dropped across

BLPRD, BLPRF & BLPRR switches are causes of higher voltage drop in the circuit because of

higher operating DC current, which in term is causing reduced availability of voltage at headlight

terminal and consequently poor light intensity is available during operation which can have safety

repercussion on line.

Therefore ELS/MGS is suggesting the above modification to be carried out in all

conventional locos.

Material required:

1. Multi core cable size 4 sq.mm about 16 meters.

2. Multi core cable size 10 sq.mm about 45 meters.

In view of above, it is requested to kindly consider the issue for 37th MSG discussion so

that modification sheet for modifying the cable size in headlight circuitry for improvement head

light intensity may kindly be issued from your end.

RDSO’s Note:

1. As per clause no. 2.3 of RDSO’s specification no. ELRS/SPEC/Dc-Dc Converter/0021

Rev. 01 for DC/DC Converter for electric locomotives, (Output supply requirements) the

rated output regulated voltage of each converter terminal should be 25.5±1% DC and

output wattage is defined as 400 W.

2. The test procedure has been laid down in RDSO Specification no. ELRS/SPEC/PR/0024

(Rev. 01) for Twin beam head light. As per clause no. 6.3.7 (Photometric test), the test

voltage at the lamp terminals shall be steady set at 24.5+0 /-0.1 V and as per clause no.

6.3.7.2 (Illumination Intensity), the lux level should not be less than 4800 lux at distance

of 8 meter.

Deliberations:

Modification suggested by ECR and the improvement in the Lux level was discussed by

the group. Calling of joint meeting of vendors for DC-DC converter & head light along with

RDSO & CLW to improve the Lux level was deliberated upon. Consistency test of DC-DC

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converter & headlight is to be carried out exploring the possibility of supply of head lamp along

with reflector as a single unit should also be seen.

Recommendations:

Consistency test of Head light/ DC-DC converter to be carried out jointly by CLW and

RDSO.

CLW & RDSO should explore the possibility of improving the design as well as supply

of headlight lamp along with reflector as a single unit.

CLW should convey a meeting with suppliers of DC-DC converter & headlight in this

regard.

Modification suggested by ECR should be implemented by Railways. RDSO should issue

necessary instructions.

Board’s decision:

Accepted.

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New Item

Item no. : 14

Subject : Problems in radial interference on DE bearing seat of

6FRA6068 Traction Motor.

Proposed by : CR

File no. : EL/3.2.182

Note of proposing Railway:

A. Minimum radial interference on DE bearing seat of 6FRA6068:

Problem:

As per RDSO/MS/0415 (Rev-0) Amendment No.1 Dt. 24.12.2013, Traction Motor

bearing seat Outer Diameter on rotor shaft is reduced in order to achieve installed radial clearance

of DE side bearing of 0.110 to 0.190 mm.

i) Original Bearing seat OD at Rotor shaft as per ABB= 180.043 to 180.068 mm

ii) ID of inner Racer measured practically on shop floor = 179.990 to 180.00 mm

iii) Range of interference practically achieved = 0.043 mm to 0.078 mm

Minimum interference of 0.043 mm is essential and less interference than 0.043 mm can

cause rotation of inner racer on shaft further resulting in bearing seizure.

1) Amended bearing seat OD of Rotor shaft as per RDSO/MS/415 = 180.028mm to

180.053 mm

2) ID of inner racer measured practically on shop floor = 179.990 to 180.000mm

3) Range of interference which can be achieved = 0.028 mm to 0.063mm

Minimum interference of 0.028 mm is very low. This can result in bearing seizure due to

rotation of inner racer on shaft.

All the sheds are getting radial clearance less than the permitted values of ABB i.e. 0.110

to 0.190 mm. This may be due to the different procedure of measurement of radial clearance.

Ajni shed is measuring radial clearance by using filler gauge whereas RDSO/ELRS/SMI-

278 Dt. 23.12.2013 recommends use of Jack and dial gauge. As per this procedure radial

clearance is measured 20 to 40 micron more than that measured by filler gauge.

Suggestion:

Original dimensions of rotor shaft at bearing inner racer seat on DE (180.043 to 180.068

mm) as per CLW’S Drg. No. 1TWD.096.009 based on original ABB document No.

3EHM112015 to be maintained.

B. Increased interference between bearing outer racer and End frame (DE side):

Problem:

As per RDSO/MS/0415 Rev-0, Amendement-1

Sr.

No

Parameter Original

dimension

Revised

dimension

Remark

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1 Inner diameter of

bearing housing in

end frame

319.943 to

320.000 mm

319.950 mm to

319.990 mm

Preferred dimension

is 319.950 mm as

per RDSO.

2 Outer diameter of

bearing actually

measured on shop

floor

319.960 to

320.000 mm

319.975 mm to

319.990 mm

Range of

interference w.r.t.

319.950 mm size is

0.025 to 0.040 mm

For bearing outer racer, lower range of interference is always preferred. Cases with 0 to 5

micron interference have worked satisfactorily in service. Up to 20 micron interference is

sufficient for outer racer. As higher interference causes rapid reduction of radial clearance of

bearing and further crackness of outer racer causes immediate bearing seizure.

Suggestion:

Nowadays all the end frames are received with ID in the range of 319.950 mm which is

not desirable as per our experience and it is suggested to recommend dimension of 319.975 mm

as the preferred dimension in place of 319.950 mm in RDSO/MS/0415- Rev- 0, Amendement-1.

RDSO’s Note:

1. Large number of failures of traction motor type 6FRA6068 bearings and its assembly

components have taken place mainly on account of the following defects:-

i. Looseness of Inner bearing stopper (NDE) inside NDE bearing bracket (End shield)

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ii. Looseness of NDE bearing inside NDE bearing bracket (End shield).

iii. Looseness of Inner bearing stopper (DE) inside DE bearing bracket (End shield).

iv. Looseness of DE bearing inside DE bearing bracket (End shield)

2. The above failures are due to insufficient interference between mating components at the

time of motor manufacturing.

3. RDSO carried out the analysis of these problems. A detailed study on concentricity &

parallelism of stators, appropriate fits and tolerances for end frame/bearing components of

Traction Motor type 6FRA6068. Manufacturers of bearings, traction motors complete and

vital components were also involved in this study.

4. Existing dimensions of components both on DE and NDE sides are such that

1. Over the range of machining tolerances, outer racer of bearings and bearing brackets

have got fits from clearance to interference, i.e. at certain combinations of dimensions

within specified tolerances; there is possibility of rotation of bearing in the end frames

due to the clearance.

2. Similarly, because of existing tolerances of inner bearing labyrinth and its seating in

end frame allow clearance to interference fits.

3 Inner racers of bearings and shaft also have only interference fits.

4. Similarly, other sets of components which should be interference fits, there

manufacturing tolerances allow clearances.

5. In the modified arrangement issued vide the MS-415 and its Amendment 1, tolerance

have been defined in such a way to ensure minimum interferences of 10 micron in all

cases.

6. After implementation of the MS-415, TM bearing failure cases have been reduced

significantly.

7. In the scenario ‘A’ given by CR (DE inner racer & shaft), interference of 28 to 78 micron

is available whereas previously it was 43 to 93 microns originally. Bearing seat

dimension of 180.043 mm is prescribed for the manufacturer which will give interference

from 43 to 68 microns.

Shaft Dia (1TWD.096.009 Alt 0) and Inner Racer of bearings DE (NU2236, SKF & FAG

make)

ID of Inner racer Shaft Dia Interference / Clearance; all negative values are

interferences and positive are clearances.

A =Min. B =Max. C = Min. D= Max E=A-C F=A-D G=B-C H=B-D

179.975 180.00 180.028 180.053 -0.053 -0.078 -0.028 -0.053

8. In the scenario ‘B’ given by CR (DE outer racer & Bearing Housing in End Shield), with

319.95 mm as preferred dimension for bore of bearing housing, interference from 10 to

50 micron is available. However, if bore is increased to 319.975 as suggested by CR,

interference of -15 (clearance) to 25 microns will be there, which is not desirable.

Outer Race of DE Bearing (NU2236, SKF & FAG make) and End Frame DE(1TWD.096.005

Alt.6)

ID of Bearing

Housing in End

Frame

OD of Outer Race Interference / Clearance; all negative values are

interferences and positive are clearances.

A =Min. B =Max. C = Min. D= Max E=A-C F=A-D G=B-C H=B-D

319.95 319.99 319.960 320.000 -0.010 -0.050 0.030 -0.010

9. In view of the above, no change is required in the dimensions specified in the MS 415

Amendment-1.

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Deliberations:

• The interference between the rotor shaft and the inner racer and between outer racer and

inner bore of end shield of traction motor were deliberated during the meeting.

• RDSO informed that adequate interference from 43 to 68 micron can be achieved

between rotor shaft and inner racer if preferred diameter of rotor shaft as stipulated in

RDSO modification sheet no.-415 is maintained.

• RDSO further informed that in few cases there will be clearance instead of interference

between outer race of bearing and inner bore of end shield of traction motor if tolerances

as proposed by CR is maintained. Hence it is desirable to maintain the tolerances as

indicated in RDSO MS-415.

Recommendations:

Group opined that there should not be any alteration in the tolerances specified by OEM

which have been in service since long.

Board’s decision:

Considering high rate of bearing failures in 6FRA6068 traction motors even after issue of

several instructions on fitment and clearances, RDSO should study in detail and address

the issue in consultation with bearing Manufacturers, Zonal Railways and audit

maintenance practices of worst affected sheds.

RDSO should issue consolidated guidelines /instructions on the issue only after full study

of the subject to avoid further confusion.

RDSO had revised critical dimensions of interference, clearances etc. vide MS 412 dated

03.10.2012.RDSO in consultation with CLW to identify if recent failures are in TM’s

with revised dimensions or not.

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New Item

Item no. : 15

Subject : Provision of LED type light for exchanging signals with

train passing staff.

Proposed by : NR

File no. : EL/0.1.3/Driver

Note of proposing Railway:

At high speed, section clearance time is very less; hence higher proportion of driver’s

time gets involved for signal exchange with station staff. After provisioning of air conditioning in

locos cabs, it will not be feasible by LP to exchange flags (Red/Green) signals with station staff

due to air tightness of cabs .To avoid this, a LED based signal exchange lamp is required to be

provided outside the cabs with control push button at the ALP/LP driver desk for exchange of

signals.

RDSO’s Note:

Running of train with manual exchange of system is for safe operation of train besides

ensuring the alertness of LP/ALP by train passing staff. The electrical signaling as proposed

cannot be alternative to manual signal exchange in any way as possibility of failure of electrical

circuit & accessories at the time when it is required most cannot be denied. The Air conditioned

cabs are having windows similar to non air conditioned cabs & windows can be opened at the

time requiring signal exchange. However, implementation of proposal requires amendment in

General Rules (1976) clause 4.40, 4.41 & 4.42 etc.

GR 4.40 LOCO PILOT AND ASSISTANT LOCO PILOT TO KEEP A GOOD LOOK-OUT.

- Every Loco Pilot shall keep a good look-out while the train is in motion and every

Assistant Loco Pilot shall also do so when he is not necessarily otherwise engaged.

GR 4.41 LOCO PILOT OR ASSISTANT LOCO PILOT TO LOOK-BACK:

- The Loco Pilot or the Assistant Loco Pilot shall look back frequently during the journey

to see whether the train is following in a safe and proper manner.

G.R.4.42 EXCHANGING OF ALL RIGHTS SIGNALS

1) All right signals are exchanged between Loco Pilot and Guard to ensure that the

Guard is in his brake-van and that the train can proceed.

2) All right signals are exchanged between Guard, Loco Pilot and Station Staff to

ensure that the train is running in a safe and proper manner.

3) The All right signal is given by holding out the green flag horizontally by day and

by waving the green light horizontally by night.

4) This signal shall normally be exchanged on the platform /station buildings side

(station limits) or left side (outside station limits) unless the track is on curve, in

which case signals be exchanged from the other side.

5) All right signal shall be exchanged as detailed below.

(i) When train starts after stopping at station.

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(ii) When train starts after stopping between stations

(iii) When train running through a station.

(iv) While passing through ghat sections.

(v) While approaching important girder bridges

(vi) When any train passing on the adjacent line / s.

(vii) When last vehicle has cleared the speed restriction zone

(viii) After clearance of the loop line cross over points, when train passes

through loop lines at a station.

In view of above, proposed modification of NR is not recommended.

Deliberations:

For changing the mode of signal exchange, necessary correction may be desirable in

General Rule for train operation or alternatively Zonal Railways may incorporate

necessary provision by making subsidiary rule.

Since same loco pilots are working in diesel trains also, the mode of exchanging of

signals by loco pilot with train passing staff/SM should be uniform irrespective of traction

to avoid confusion in the mind of operating staff.

Recommendations:

The group was not in favour of this modification. Since, it involves modification in GR. It

is also pointed out that, it needs more deliberation and consultation with safety

department also.

Board’s decision:

Accepted.

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New Item

Item no. : 16

Subject : Introduction of ‘H’ type tight lock coupler with soft

draft gear in Electric locomotives.

Proposed by : Railway Board

File no. : EL/3.2.119 (CBC)

RDSO Note:

1. There are two main parts in ‘H’ type tight lock coupler with soft draft gear, i.e. ‘H’ type

tight lock coupler assembly (specification no. MP-0.41.00.05) and Soft draft gear with

Yoke assembly (specification no. MP.0.41.00.06).

2. These couplers were provided in WAP-4/WAP-5 and WAP-7 locomotives. However due

to smaller pocket size in WAP-5 and WAP-7 locomotives, the soft draft gear as per initial

drawing could not be fitted. As such the drawing was revised and overall length of soft

draft gear has been reduced by 40 mm to avoid infringement with loco body while in buff

mode. This smaller size of draft gear has been fitted successfully in WAP-5/WAP-7

locomotives at ELS/Ghaziabad and CLW

3. It is proposed to cut-in ‘H’ type couplers in all Locomotives manufactured in CLW and

‘E’ type coupler should be replaced by ‘H’ type coupler during POH of

conventional/three phase locomotive by the workshops.

Deliberations:

RDSO presented that ‘H’ type coupler has been successfully provided on WAP5/WAP7

locomotives. Northern Railway pointed out the problem of fitment of draft gear of M/s Faively

make in WAP7 type of locomotive and the drooping problem of M/s Faively make couplers.

RDSO should study the design and sort out these problems.

Recommendations:

‘H’ type tight lock coupler should be used on passenger locomotives. CLW to cut-in these

couplers in regular production.

‘H’ type tight lock coupler should be provided by POH workshops/Sheds during major

schedules.

Board’s decision:

Accepted.

RDSO to resolve all issues related to fitment & performance raised by Zonal

Railways in consultation with MP dte.

All instructions related to fitment designs specification, maintenance manuals and

any other technical instructions of H-Type tight lock coupler should be circulated

to all Railways.

Railways to report performance feedback for such couplers on regular basis to

RDSO MP & Electrical dte.

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New Item

Item no. : 17

Subject : Use of Composite Brake Blocks.

Proposed by : Railway Board

File no. : EL/3.2.19/5

RDSO Note: Earlier, the cast iron brake blocks were used in all electric locomotives. Later on decision

was taken to switch over to composite brake blocks in place of cast iron brake blocks.

Railways highlighted wheel breakage/gauge widening cases with the use of composite brake

block in electric as well as diesel locomotives.

This matter was discussed in the meeting held at Railway Board which was also attended by

officers of Electrical & Motive Power Directorates of RDSO on 05.10.2009. In the meeting

decision was taken to switch back to cast iron brake blocks in WAG7 locomotives and

Railways were advised the same vide RDSO letter no. El/3.2.19/5 dated 31.08.2009 except

WAM4 & WAG5 loco.

Considering the relief in the failures of wheel disc, due to usage of cast iron brake block

decisions were taken in different meeting to use cast iron brake block on all types of electric

locomotives.

It is worthwhile that earlier the procurement of composite brake block were carried out as

per MP directorate specification no. MP.0.01.00.04 (Rev - 06) of May’ 2007 & (Rev - 07) of

July’ 2008.

Meanwhile specification no. MP.0.01.00.04 (Rev - 08) of Oct’ 2008 of composite brake

block has been revised and some important changes in the specification were carried out to

improve the quality of the composite brake block such as:

i) Composition of the material constituting the brake block must be chosen to give proper

heat dissipation of heat generated at wheel and brake block interface.

ii) Max. temperature occurred due to prolonged braking has been reduced from 3750C to

2750C.

iii) Maximum 30% of the values of mean coefficient of friction may fall below the lower

limit of the band. The tolerance bands of the mean coefficient of friction shall be as per

Annexure-II of the above specification.

iv) Value of hardness (85R to 115R), back plate pull off strength (less than 4T) & acetone

extract (not exceed 3%) of composite brake block is specified.

v) Testing procedure of composite brake block has been specified in Annexure VIII of the

specification where in test methods to check the mechanical physical & chemical

properties like Density, Hardness, Modulus of Elasticity (compression), Cross breaking

strength, Acetone extraction, and Ash content has been specified.

As per MP directorate instruction bulletin no.MP.IB.BK.02.16.08, brake cylinder pressure

was reduced from 2.5 kg/cm2 to 1.8 Kg/cm² during application of automatic brake valve by

A-9 to reduce the brake power on loco.

In the meantime the diesel locomotive continued with the composite brake block. After

consultation of MP directorate/RDSO it has been experienced that the initial problem of

gauge widening which was experienced in the diesel locomotive has been overcome and now

no such problem are being faced by them.

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It is understood that after revision of the specification the quality of composite brake block

has been improved which could be a reason of satisfactory performance on the diesel

locomotives.

Apart from the above, following facts are being brought to notice for use of composite brake

block:

(i) The maximum wheel temperature rise as per dynamometer test report of composite brake

block vis a vis cast iron brake block are comparable as brought out in different reports

given by testing directorate as stated below:

SN Report No. Wheel disc fitted with Cast

iron brake blocks

Wheel disc fitted with

composite brake blocks

Max. Wheel Temp (0C) Max. Wheel Temp (

0C)

1 M-346 125 150

2 M-365 150 187

3 MT-39 237 211

4 MT-133 214 162

5 MT-1198/MT-1163 165 194

(ii) The service condition for electric and diesel locomotive are only slightly different in

terms of load being hauled by electric locomotive is more than hauled by diesel

locomotive. However drivers are counseled to release loco brake during braking of the

train.

(iii) Because of less tear and wear life of the wheel will also increase.

(iv) Cast iron brake block are also prone to theft.

(v) The life of composite brake block is more compared to cast iron brake block hence

frequent changing is not required. Also handling of composite brake block is easier due to

less weight.

(vi) It is also understood that besides technical justification, the commercial rate of supply to

Indian Railways of cast iron brake block are nearly two times that of composite brake

block.

(vii) Therefore, after reviewing the usage of cast iron brake block in light of composite brake

block being used on diesel locomotive it has been decided to use of composite brake

block on all type of conventional locos including WAP7 locomotive and the same has

been instructed to Railways vide RDSO letter no. EL/3.2.119/5 dated 15.012015.

Deliberations:

RDSO presented the modification carried out by MP directorate in the specification of L

type composite brake block to improve the quality of composite brake block. Some of the

Railways (NR & WCR) has already provided composite brake block which are running

for the last 3 to 4 months. RDSO has send a proposal to MP directorate to reduce the

brake cylinder pressure to 1.2 Kg/cm2 to reduce the braking force on locomotive during

A9 application if the loco pilot fails to apply PVEF.

MP directorate is also working on development of composite brake block of WAG9

locomotive.

Recommendations:

Railways to use composite brake block on all conventional locomotives as well as on

WAP7 three phase locomotive and sent regular feedback to RDSO.

RDSO to expedite development of composite brake block for WAG 9 locomotive.

Board’s decision:

Accepted.

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New Item

Item no. : 18

Subject : RDSO & CLW to jointly give a presentation on status of

reliability improvement measures taken for IGBT

propulsion.

Proposed by : Railway Board

File no. : EL/11.5.5/1/IGBT

RDSO Note:

1. Reliability issues of M/s ABB make SR & BUR:

Failures of power module:

Failures of power module of M/s ABB are very high as there had been 9 failures in 2013-

14 and 25 failures of power module reported during 2014-15 (up to Jan-2015). Firm has

submitted investigation report of two modules being Sr. No. HYPK 04 & IAHH 18, which

indicates flaw in manufacturing process (particle impurity in the IGBT conduction area & thermal

paste was missing from the screw holes).

Firm has submitted action plan to weed out suspected lot of 38 nos of IGBT from service

from two locos from 31401 (ELS/BIA) & 31470 (ELS/AQ).

Failures of Duagon module:

The failures of Duagon cards in SR are alarming. Firm has identified root cause of failure

as firmware. With the changed firmware six (06) locos nos. 31420, 31404, 31536, 30395, 30400

& 35567 have been provided with modified Duagon cards for trial and observations. Railways

and firm should closely monitor the performance of Duagon Cards w.r.t life sign missing

message. This should be first established and then only further proliferation of dugaon card’s

latest Firmware will be done in all locomotives. Feed back to RDSO and CLW was to be given.

Failures of PEC-800 cards:

Firm had identified the root cause of failure as “flash memory corruption, port problem

and use of wrong PEC tool”. These issues have been addressed in latest software version-35 a

alpha provided in 69 locos out of 75 locos. The performance in field needs to be monitored and

feedback to be given to RDSO and CLW.

Software issues:

To reduce the initialization timings (67 sec):

a) The mismatch of clock timings of SR/BUR and VCU has been a regular feature in

service. Firm had confirmed that the latest software version 35 will be able to maintain

the timings. Railways to monitor and give feedback to RDSO and CLW.

b) Implementation of DDS message in DIA cards of VCU is yet to be done. Firm has been

advised for immediate compliance failing which further commissioning and supplies of

SR will be stopped. A feedback to RDSO and CLW should be given by M/s. ABB.

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c) The other parameters like failure of regenerative braking during first instance, individual

traction motor isolation, change over between FLG-1/2 required to be resolved

immediately. The software version 35 which is a latest of M/s. ABB needs to be

monitored very closely.

d) A large number of failures of components mainly IGBT module and electronic cards are

taking place during the commissioning of new SR in CLW itself. There is a need to

improve and strengthen the final testing by the manufacturer in their own premises before

dispatch.

The adequate stocking of spares: Firm for compliance of warranty obligation had not been

done by the firm so far. PDC is 30.5.15. ELS should ensure and give feedback.

2. Reliability issues of M/s. BHEL make SR & BUR:

Failures of power module:

Firm had implemented modifications named as P-1, P-2 and P-3. It has been observed

that even after completion of P-3 modification in all units, 15 nos. of failures of IGBT module has

been reported. BHEL has indicated that most of these failures are due to poor workmanship

during implementation of P-3 modification. It was decided in the meeting held at CLW that firm

to draw a concrete plan to avoid the failures and to submit to RDSO and CLW immediately.

Action Plan not yet submitted.

Failures of DCU cards:

They have been 25 Failures of DCU card during 2014-15. Firm has been advised to

submit investigation report. Investigation report is still awaited.

Coolant leakage:

Railways have reported cases of leakage of coolant which is primarily due to poor joints

and overall workmanship of cooling system.

Firm submitted a proposal for providing flange coupling in place of screw coupling. This

has been cleared by RDSO and to be trialed in 10 locos before regular implementation.

Software related issues:

a. A large number of failures have been reported due to ASC pulsing stop. The firm has

indicated that with the modification in software version 366, this problem will get

resolved. However, it is seen that the findings and investigation of the cause is not based

on the feedback and factual conditions on line. Firm had related this problem with neutral

section whereas this is not true as large numbers of cases are even reported without any

neutral section during running.

M/s BHEL uploaded modified software in loco no 31431 of ELS/KYN on 28/04/2015.

There is no failure reported so far.

b. Momentary Problem of Harmonic filter getting isolated: Harmonic filter getting isolated with message SLG1:0073- Contactor 8.1 stuck on &

SLG1:SLG1:0059-Contactor 8.1 stuck on fatal is being observed in loco no. 31248 and

30313 locos of ELS/LGD. BHEL was advised to carry out joint investigation with

ELS/LGD and submit report. Joint report is still awaited.

c. Measuring of battery charging current needs to be reviewed for proper messages.

Presently, the message comes when battery voltage already gone below 92 V. M/s BHEL

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has informed that this problem is being addressed in BUR software version 983.3 which

is put under trial at ELS/BIA.

d. The failure of ACI module of BUR:

Failures of ACI cards have increased. Firm indicated that sometimes, on Power-ON of

Aux Converter, some specific ACI modules enter “Safe Mode” reporting Boot-Loader

Mode and Bogie gets Isolated. Firm indicated that improvements are made in FPGA

software of ACI module to prevent Boot-loader error due to simultaneous read/write

conflict. This improvement is now available as FPGA image Version 0.05 and the error is

arrested.

M/s BHEL has informed that this problem is being addressed in BUR software version

983.3 which is put under trial at ELS/BIA.

Poor stocking of spares: The overall performance of BHEL has been very poor and

response is highly sluggish in warranty repairs and replacement of equipment. This was

decided in ELS/TKD to stock spares by 31-5-15. No action plan has been given.

3. Reliability issues of M/s. BTIL make SR:

i) The population of BT make SR is 30 nos. M/s. BT had completed the modification for

cable crimping in all locomotives which was resulting into erroneous over current

messages in BUR and there has been no repetition of failure. However, Sheds should

monitor and give the feedback.

ii) The latest software version 1215 has been downloaded in 12 locomotives and

performance reported to be satisfactory. To be completed in all locomotives.

iii) The software version 1215 has addressed the issues of multiple software in VCU, FLG

software modified to give 510 kNT in WAG-9H locomotive.

iv) Firm had carried out the trials for confirmation of 510 kNT T.E. in WAG-9H loco in

association with CLW. The results were found to be satisfactory. However, the results are

to be sent to ELS/GMO/ECR for further evaluation and assessment of their effectiveness.

If required, one more such trial will be carried out by BT and CLW jointly in association

with ELS/GMO.

v) It has been reported by Railways that M/s. BT has sue moto modified the software of

VCU for making it compatible with their make SR. This has resulted into non-

standardization of VCU software. In case of need for replacement of control card of

VCU, their software is required to be changed every time. This is a serious issue and

adversely affecting the interchangeability of VCU and its cards. M/s. BT is required to

address the issue and advised not to change VCU software without prior approval of

RDSO and CLW. The changes already made by them are required to be reviewed by BT.

Till such time, the maintenance staff in ELS are to be trained and updated by BT to

maintain clarity.

vi) The adequate stocking of spares for compliance of warranty obligation had not been done

by the firm so far.

4. Issues with M/s CGL make SR:

i) Only 01 no. SR is under trial in WAG9 loco No. 31412 at ELS/GMO/ECR. Most of the

tests have been completed and under evaluation at RDSO for issue of clearance of

prototype.

ii) M/s. CGL to address the issues of booting time less than 50 sec which is 2 minutes at

present. Recording of DDS data in DIA card of VCU and other software issues for better

reliability of the SR to be ensured.

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5. Other Reliability improvement Measures:

i) CLW has framed and issued specification No.CLW/ES/3/IGBT/0486 Alt.’D’ for IGBT

traction converter which is having standard layout, orientation and provision of cables, motor

terminals and other functional aspects of traction converters. Manufacturers have been

requested to submit their design and start manufacturing with the revised specification even

during the supplies against existing P.Os.

RDSO shall issue revision in their specification of complete propulsion system of 3-phase

locomotives incorporating the details needed for standardized layout as per CLW revised

specification of traction converter. Specification has been revised and uploaded on RDSO

website on 19-7-15 for seeking comments.

ii) Similarly, the standardization of layout / design for auxiliary converter (BUR) have to be

adopted. CLW had already placed draft revised specification on CLW website. Specification

will be issued after finalization.

iii) TCN compliant Open Control VCU has been successfully developed by C-DAC. CLW had

entered into a MoU with C-DAC for ToT and proliferation of the VCU in 3-phase

locomotives. EOIs have been called and manufacturers have shown interest in development.

CLW is analyzing their offers against EOIs.

Deliberations:

RDSO and CLW made a presentation on the reliability improvement measures already

taken as well as under implementation/ under field trial for IGBT based converters.

Railways informed that though there is improvement in the reliability of IGBT based

converters with implementation of reliability action plan / modified software. However

field performance of locomotives provided with modified software are required to be

monitored and pending issues are to be resolved by the manufacturers. Group opined that

there has been a reduction of failure during first quarter of current year as compared to

previous year.

Group has been informed that M/s ABB has uploaded modified software in one

locomotive of ELS/TKD/WCR and 04 locomotive of ELS/Bhilai/SECR. This has been

done to address the problem of logging of DDS massage in DIA card of VCU & other

software related issues. Railways (WCR & SECR) have reported satisfactorily field

performance of locomotive provided with modified software. Few issues are still to be

resolved.

RDSO informed that Railways to monitor the performance of converters provided with

modified software by M/s ABB & M/s BHEL and submit feedback so that action on

further proliferation may be taken.

CLW informed that a web page has been created on CLW website giving details of

reliability measures under implementation by various firms.

Recommendations:

Railways to furnish performance feedback to RDSO/CLW for modified software to

address the issue of data recording in DIA card of VCU & modified software of duagon

card of M/s ABB.

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Based on performance feedback of Railways, RDSO/CLW may take action on further

proliferation.

RDSO/CLW to coordinate with M/s ABB for compliance of pending issues and meeting

with M/s ABB may be convened in October’2015.

Railways (CR & SCR) to give feedback of software version-366 of M/s BHEL which is

under field trial in locomotive of Kalyan and LGD sheds. SECR to give feedback of BUR

software version 983.3 of M/s BHEL, which is put under trial at ELS/BIA.

CLW to upload loco-wise/date-wise modification details on its web page. Details/Salient

features of software versions may also be provided on the web page.

Board’s decision:

Accepted.

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New Item

Item no. : 19

Subject : Presentation by SE Railway on benefits of using WAG9

MU in place of WAG7 MU.

Proposed by : Railway Board

File no. : EL/3.1.35/2(Elect.)

Note of proposing Railway:

Traction Energy Conservation through coasting and regeneration:

Traction Energy Conservation:

• Approximately 97% of the Freight Traffic and 90% of the Passenger Traffic on South

Eastern Railway (SER) is run on Electric Traction.

• Total energy consumption of 1470 Million Units amounting to approximately Rs.900

crores/annum, which constitutes about 13% of the total working expenses of SER.

• There is an immense potential of energy conservation of traction energy alone on SER by

way of coasting and re-generation (in 3 phase electric locomotives).

Advantages of WAG9 MU over WAG7 MU:

Average speed of 26km/h with WAG9H MU is achieved compared to 24 km/h with

WAG7 MU despite load being higher by 400 tons and maximum speed limited to 45

km/h in the former against 60 km/h in the latter.

Average energy consumption is about 23% less compared to WAG7 MU loco, resulting

in saving of about Rs. 1.4 crore per train per year.

Reduce wear & tear of track by use of regenerative braking.

Reduce wear and tear of wheels and brake blocks.

ROAD MAP TO SAVE ENERGY:

Large scale induction of three phase locomotives both in freight and coaching services for

increased throughput and energy efficient train operation.

Sensitization of Loco Pilots and Assistant Loco Pilots for energy conciousness.

Deliberations:

Railways stated that owing to availability of regenerative braking in 3-phase

locos; the scheme is beneficial by saving of energy & avoiding early replacement

of brake blocks.

Bench marking of SEC should be done route-wise / load-wise for general

awareness regarding energy conservation over running staff.

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Recommendations:

The group has recommended for adopting of scheme.

Board’s decision:

Accepted.

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New Item

Item no. : 20

Subject : Improvement in adhesion of WAG9 locos by providing

additional sanders and increasing efficiency of sanding

operation.

Proposed by : Railway Board

File no. : EL/3.2.19/3-phase

RDSO’s Note:

SUBJECT:

There are cases of stalling of WAG-9 Locos during Monsoon / Rainy season. Though

capacity of sand box has already been increased from 24.6 to 35.5 Litre and cut-in by CLW in

2010, however it has been observed that sometimes during Monsoon / Rainy season actual

Tractive Effort is less than the desired Tractive Effort due low adhesion between the rail and

wheel thus preventing wheel slipping by the traction converter software by reducing the Tractive

Effort.

In conventional locomotive in similar situation drivers normally keep on applying tractive

effort with slight wheel slipping. This slight wheel slipping improves the adhesion. However such

control in 3phase locomotive is neither with the driver nor it is built into software.

Constraints:

1. Sanders are fed from a 5ltr reservoir (Item 170). The capacity of the reservoir is very

less. In conventional locomotive sanders are fed directly from Main Reservoir.

2. The 5ltr reservoir is fed from a chock of 1 mm (Item No 171). The air pressure in

5ltr reservoir does not maintained for more than 5 second as soon as sanders start

working.

3. In WAG9 locomotive only 4 wheels are provided sanders in one direction of travel.

Any sanders not working shall lead to the wheel slipping.

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Wheel No. 2/5: ADDITIONAL SAND-BOX & PIPES

PROVIDED

RDSO’s Recommendation:

1. To improve the working percentage of sanders, 8 Nos. of sanders are

proposed to be provided on Middle wheel ie No. 2 & 5 wheel (one for each

direction) in line with AC/DC locomotive sanders.

2. Existing 1 mm Choke (Item No. 171) is provided in 5 Ltrs Sand reservoirs

(Item No. 170) same to be Removed and 5 mm chokes to be provided to

avoid the starvation of air within 3 to 4 seconds. This may be done in 05

locos initially to monitor field performance and MR pressure drop due to

higher size of choke.

ELS/KLY/CR has provided 16 Nos. Sanders on Loco 31418 and 5 mm choke provided in

Item No. 171 and Sanders working checked found all 8 Nos. in each direction working

satisfactorily for 1 to 2 minutes continuously without any trouble.

Deliberations:

• RDSO informed that sanders are fed from a 5 litres reservoir, which was fed from a chock

of 1 mm. Choke size has already been increased from 1 mm to 3 mm in 2006. Railways

have been advised to verify the same and increase the size if not done.

• ELS/KLY/CR proposed for provision of 5 mm choke in place of 3 mm and informed that

shed has provided 8 Nos. of additional sanders on Middle axles i.e. No. 2 & 5 (one for

each direction) in line with AC/DC locomotive sanders on Loco 31418 a& 5 mm choke

provided and sanders working checked, found all are working satisfactorily for 1 to 2

minutes continuously without any trouble.

• RDSO informed that provision of 5 mm choke in place of 3 mm will increase the flow

rate by 2.8 times (25/9) and may lead to MR air pressure drop.

• Group opined that this may be done in 05 locos initially to monitor field performance and

MR pressure drop due to higher size of choke.

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Recommendations:

CR (ELS/KLY) to provided 8 Nos. of sanders on Middle wheel i.e. No. 2 & 5 wheel (one

for each direction) in line with AC/DC locomotive sanders with 5 mm chock in 05 locomotives

for field trial and monitor the performance and MR air pressure drop and submit report to RDSO

for further action.

Board’s decision:

Accepted.

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New Item

Item no. : 21

Subject : Procurement of spares from OEM’s-Implementation of

life cycle cost concept to obtain reasonable prices and

long term support from OEM’s.

Proposed by : SCR

File no. : EL/2.1.8

RDSO’s Note:

Procurement of major items whose maintenance spares are procured in the form of

kit may be done taking in to account the cost of AOH/POH kit. This will help in

economical cost of maintenance and procurement of new items.

SCR may give presentation.

Deliberations:

AML has opined that Railways may enter into 5 or 7 years AMC at the time of

procurement of major equipments.

Railways suggested that breakup of cost of individual items may be asked at the

time of procurement.

Recommendations:

CLW should explore the possibility of procurement of new equipment along with

the cost of AOH/IOH/POH kit and spares.

Board’s decision:

Accepted.

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Part-II

Discussion on Status/Compliance on Decision on items of 36th

MSG (Elect Loco)

Meeting held at IRIEEN, Nasik Road on 21st & 22

nd Nov’ 2013

Item

no.

Subject Recommendation of

MSG

Board’s

decision

on

recomme

ndation

of MSG

Status/Action taken

1 (a) Performance of

VCD-

(i) Evaluation of

performance for

different makes of

VCDs and

implementation of

reliability Action

Plan in a time bound

manner.

(ii) Reliability of

VCD’s along with

road

map/improvements

required to link

isolation of VCD to

loco withdrawal

from service.

(iii) Standardization

of VCD displays

parameters &

Electrical isolation

of VCD main unit

from control circuit.

(iv) Control circuit

of VCD.

(b) Notes by SR:

(i) In order to avoid

confusion to running

staff as well as

maintenance Staff

the display message

are to be made

uniform in all makes

of VCDs.

(ii) To avoid wrong

feeding due to short

circuiting it is

suggested that VCD

main unit control

cards are to be

electrically isolated

using opto couplers.

(c) Notes by NR:

In case, 110 volt DC

supply of VCD

(a)Railways to initiate

immediate procurement

actions for spares from

respective manufacturers.

(i) VCD is just an aid to the

loco pilots and its functioning

in locomotive is to assist

them in performing their

duties nonfunctioning of

VCD shall be recorded in the

loco logbook and shall be

attended in the base shed but

locomotive shall not be

declared failed in case of fault

in VCD. In case spares of a

particular make are not

available with a Railway or

locomotive shall not be

detached for attention. The

VCD must be attended in

next schedule in home shed.

(ii)RDSO to take up the

reliability issues and

implementation of RAP

already decided with the

manufactures regularly

involving Railways.

(iii)As per the specification,

items to be procured from

CLW/RDSO approved

sources should be procured

by the manufactures from

Part1 & Part II approved

sources only in the ratio

prescribed in stores code.

This should be made part of

procurement contract by

Railways.

(iv)RDSO has issued

Reliability Action Plan (RAP)

Accepted

along with

following:

Decision

on

permitting

loco with

defective

VCD shall

be taken

by

Railways

individuall

y till

reliability

of VCD’s

improveme

nt up to the

acceptable

level.

Regular

feedback

from

Railways

to be

ensured by

RDSO.

Based failures collected from Zonal

Railways, a reliability improvement

meeting of suppliers and Zonal

Railways were held at RDSO. MOM

has been issued vide VCD letter no.

EL/3.1.14 dated 09/06/2015.

M/s Stesalit have been temporarily

delisted as not responding.

As the reliability issue is still there,

this item is being taken up in the 37th

MSG meeting.

RDSO vide letter no. EL/3.1.3 dated

12/08/2015 issued the Technical

Circular no.

RDSO/2015/EL/TC/0131, Rev ‘0’

dated 04/08/2015.

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circuit is controlled

through CCBA fuse

(wire no.003), the

whole loco will be

shut down due to

any fault in VCD

circuit, and shall be

difficult for driver to

trouble shoot the

defective circuit.

Therefore it is

necessary that VCD

circuit should be

controlled either by

another fuse like

CCLC, CCLS or

CCLF1/2) or by

providing separate

glass fuse in Cab-1

SB.

vide this office letter No.

EL/3.1.14 dated 13/08/12.

Further for Stesalit Make

VCDs, other reliability action

plan was circulated vide this

office letter no. EL/3.1.14

dated 22/01/13. Railways

should submit progress of

RAP separately for each

make so that concerned

supplier may be taken up by

RDSO. It is also requested

that Railways should also

send performance report and

RAP progress in editable

Excel form as softcopy at

[email protected].

(b)No change is required in

display messages.

(c)RDSO to issue necessary

instruction to railways in this

regard.

2 Reliability of various

speed sensors

provided in 3-phase

locos and their

maintenance issues;

and increase in

resistance value of

temperature sensor

cable shielding.

Notes by CR:

Increase in

resistance value of

temperature sensor

cable shielding.

(a)

• This is a CLW controlled

item. CLW/RDSO to monitor

the performance of modified

speed sensors of M/s. ARC.•

CLW/RDSO to develop

automatic change over

provision of two channels of

speed sensors so as to achieve

hot redundancy.

• CLW/RDSO to develop

new type of speed sensors for

GTO locomotives having

power supply and output

signal module external to

sensor box.

(b)

•CLW to amend the

specification to provide

connection of shielding to E-

pin of the female connector

and on the gland of traction

motor side.

• CLW to provide connection

of shielding of cable to E pin

of male connector on the

junction box.

• RDSO to issue SMI in this

regard for existing

locomotives.

Accepted. 1. New Type of sensor having power

supply outside has been

developed by M/s ARC and

provided to ELS/LGD (Two sets)

and ELS/GMO (One set) for field

trial. These speed sensors were

provided on 10-7-14 & 24-10-14

on two locomotives of ELS/LGD

and on 22-12-14 at ELS/GMO.

Performance of these speed

sensors have been reported

satisfactory by both the Railways.

Zonal Railways have been advised

by RDSO: To replace all double

channel speed sensors by single

channel with power supply

outside; and To replace single

channel speed sensors already in

service, which are under

warrantee as on date of MOM

dated 12&13-6-14 and onwards,

by single channel modified

sensors with power supply

outside.

2. RDSO has issued the

modification sheet no.

RDSO/2015/EL/MS/0437(Rev.0)

dated 14.01.2015 to avoid failure

of temperature sensors due to

increase in resistance value of

temperature sensor cable

shielding.

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7 Software

modification

including adhesion

improvement.

1) Railway to implement the

software modifications

already cut in on priority.

2) SCR,ECR & CR to give

trial report of the software

modifications of Monitoring

of contactors 52.5/1.2 (oil

pumps) and 52.4/1.2

(scavenge blower) and

generating appropriate

message without requiring

any additional wiring and

Starting of BUR-2 at 50 Hz

directly to RDSO.

3) CLW to issue software

release notes of all the

software modification done

so far with software

version/date to Railways.

4) RDSO to do trials of

software modifications done

with the help of BT on

priority and release the

software.

Accepted. M/s BTIL has informed that adhesion

improvement software shall be done

in WAP7 locomotives on chargeable

basis.

8 Multiple Operation

of Tap-changer

Locomotives Fitted

with MPCS

Locomotives and

other Reliability

Improvement

Measures Taken in

Ver-2.

1) RDSO will explore the

possibility of use of signals

available in digital notch

indicators in the control logic

of MPCS, otherwise encoder

shall be used for sensing of

positions of SMGR.

2) Provision of serial

communication between two

MPCS fitted locomotives for

multiple/consist formation,

irrespective of make through

full duplex RS 482 serial

communication shall be

implemented.

3) Additional LSGR in

locomotives with relay logic

shall be implemented to avoid

the problem of mismatch of

notches.

4) Possibility of display exact

notch position of rear

locomotives in Ver-3 of

MPCS shall be explored and

if possible shall be

implemented.

Accepted. 1. Encoder used in sensing of

SMGR notches in MPCS ver-3

2. Serial communication provide in

MPCS ver-3.

3. Addition ELGR display provided

display screen of MPCS ver-3.

Exact notch position of rear loco

provided in MPCS ver-3.

9 Development of SIV

Units with

Redundancy for

Tap-Changer

Locomotives.

•A committee comprising of

RDSO (DSE/PS&SC) and

Sheds (Sr.DEEs of

ELS/GZB/NR,

ELS/MGS/ECR &

ELS/TKD/WCR) to be

formed to discuss &

formulate the functional

specification requirement of 2

X 150 KVA Static converter.

• RDSO to prepare

Accepted. As per decision taken during 36th

MSG draft (FRS) functional

specification requirement (FRS) has

been prepared. A meeting with

committee comprising of RDSO

(DSE/PS & SC) and Sheds (Sr.DEEs

of ELS/GZB / NR, ELS/MGS/ECR

& ELS/TKD/WCR) has been held.

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specification as per laid down

guidelines.

10 Development of

functionally

equivalent

electronics for 3-

phase locomotives.

RDSO to take up this

development on priority.

ToT partners have been advised to

develop functionally equivalent cards

however no proposal has been

submitted.

11 Defining codal life

of Electronic

equipments and

electronic modules

in 3-phase

locomotives.

A committee of SAG officers

of RDSO, Railway Board,

CR, and ECR & SCR with a

finance officer of Railway

Board should be formed.

Accepted

along with

following:

'RDSO to

submit terms

& references

to get

nomination

of officer

from board

(finance)

accordingly.

Committee of SAG officers of

RDSO, Railway Board, CR, and

ECR & SCR with a finance officer of

Railway Board to be nominated by

Railway Board.

12 Problems on Bogie

clearances of 3-

phase locomotives.

1) A team of officers of

RDSO and CLW will visit

ELS, BRC for Root Cause

Analysis of the problem of

less buffer height in WAP5

locomotives and will submit

their recommendations by

Dec 15th 2013.

2) For WAG7 locomotives,

CLW shall arrange weighing

of at least five WAP7

locomotives by the first week

of December’13.

3) RDSO and CLW will

jointly study the problem of

abnormal clearances in bogies

of WAP7 locomotives,

including audit of

manufacturing process of all

relevant components at CLW

and its approved vendors,

This will include the study of

TC-0082. The team shall

submit their report along with

recommendation by Jan 15th

2014.

Accepted. RDSO official has visited at

ELS/BRCY on 07.04.2014 &

08.04.2014 to examine the issues

related to less buffer height in WAP5

locomotives. During the visit,

measurements of buffer height on

level track have been carried out on

two WAP5 loco no. 30052 and

30070 which are received from CLW

and some certain deficiencies were

observed.

To minimize the subject issues, CLW

has been advised some corrective

measures vide this office letter no.

EL/3.1.35/2 (brake lever) dated

20.11.2014 & 17.10.2014.

Further the committee is looking into

this problem.

15 Modification in IP

magnet valve circuit

(from cable 003

instead of cable no.

700)

RDSO shall issue necessary

modification sheet with

proper rating of CCLS fuse.

Accepted. RDSO vide letter no. EL/3.1.3 dated

12/08/215 issued the Technical

Circular no.

RDSO/2015/EL/TC/0131, Rev ‘0’

dated 04/08/2015.

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Page 76 of 76

CONCLUDING SESSION

At the end of meeting, Addl. Member (Elect.) expressed happiness over the useful

deliberations, which took place during MSG meeting. He hoped that CELEs and Sr.DEEs

would continue to give their ideas/suggestions to solve operational and reliability issues.

He also complemented CEE/NR and his team for making nice arrangements for the

meeting.

Next MSG Meeting:

It was unanimously decided that the next 38th MSG (Elect. Loco) meeting will be held at

South East Central Railway.

Vote of Thanks:

Shri Om Prakash Kesari, EDSE (Co-ord)/RDSO proposed the vote of Thanks.